Accident Details
Probable Cause and Findings
A directional upset on landing due to a thermally induced atmospheric disturbance, which the pilot was unable to successfully counter due to improperly set rudder travel limits.
Aircraft Information
Registered Owner (Current)
Analysis
HISTORY OF FLIGHTOn May 13, 2016, about 1315 Pacific daylight time, a Cessna 180, N9370C, was substantially damaged when it nosed over onto its back following a landing at California City airport (L71), California City, California. The private pilot and his passenger received minor injuries. The personal flight was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed.
According to the pilot/owner, the airplane had just been approved for a return to service via an annual inspection the day prior to the accident. Subsequent to that, the pilot conducted one uneventful flight in the airplane. The following day, the pilot and his passenger flew from Shafter Minter field (MIT), Shafter California, to L71, in order to have another maintenance facility provide a cost estimate for some sheet metal work. The flight was uneventful until the landing on runway 24. The airplane touched down in the three-point attitude, bounced once, and then touched down again. Immediately after touchdown, the airplane began veering to the left, but the pilot was unable to correct the veer, despite control inputs and right brake application. When the airplane had slowed to a speed between 15 and 10 mph, it exited the south edge of the paved runway surface, and nosed over onto its back.
Personnel from two separate airport maintenance facilities were summoned to right the airplane, and clear it from the runway environment. The individual who was to conduct the sheet metal work was an aircraft mechanic with an Inspection Authorization, and he assisted in the recovery. He reported that prior to righting the airplane, he manually rotated both main wheels in both directions; they rotated freely, and offered only normal resistance. The airplane was then righted, and towed backwards on its main gear to his facility. On-scene documentation indicated the presence of a skid mark that terminated at the edge of the pavement, and aligned with the right main gear. The skid mark was estimated to be about 300 feet long. The airplane was retained undisturbed for subsequent examination by Federal Aviation Administration (FAA) and NTSB personnel. PERSONNEL INFORMATIONThe pilot held a private pilot certificate with an instrument rating. He reported that he had about 1,430 total hours of flight experience, including over 1,000 hours in taildragger airplanes, and 105 hours in the accident airplane make and model. His most recent flight review was completed in April 2015, and his most recent FAA third-class medical certificate was also issued in April 2015. AIRCRAFT INFORMATIONFAA information indicated that the airplane was manufactured in 1955, and was equipped with a Continental O-470 series engine. The airplane was involved in a landing accident in 1974 but was repaired and returned to service.
The pilot purchased the airplane in May 2015. According to the pilot, the airplane and engine had a total time in service of about 2,271 hours.
The most recent annual inspection included some brake maintenance. Both brake discs, and the left brake pads, had been replaced with new components; the previous/used brake pads were retained on the right brake caliper. Comparison of the maintenance entry writeup and the airplane manufacturer's maintenance guidance indicated that the components that were replaced were the correct part numbers. No other potentially relevant activity was noted in that annual entry. METEOROLOGICAL INFORMATIONThe 1320 automated weather observation at Mohave Air and Space Port (MHV), Mohave, California, located about 9 miles southwest of L71, included winds from 200 degrees at 15 knots, visibility 10 miles, clear skies, temperature 32 degrees C, dew point minus 4 degrees C, and an altimeter setting of 30.00 inches of mercury. AIRPORT INFORMATIONFAA information indicated that the airplane was manufactured in 1955, and was equipped with a Continental O-470 series engine. The airplane was involved in a landing accident in 1974 but was repaired and returned to service.
The pilot purchased the airplane in May 2015. According to the pilot, the airplane and engine had a total time in service of about 2,271 hours.
The most recent annual inspection included some brake maintenance. Both brake discs, and the left brake pads, had been replaced with new components; the previous/used brake pads were retained on the right brake caliper. Comparison of the maintenance entry writeup and the airplane manufacturer's maintenance guidance indicated that the components that were replaced were the correct part numbers. No other potentially relevant activity was noted in that annual entry. WRECKAGE AND IMPACT INFORMATIONThe airplane came to rest inverted, on a magnetic heading of approximately 025 degrees, in the desert soil just off the south edge of the runway. The outboard end of the left wing extended onto the paved surface. The stopping point was located about 1,800 feet from the 24 threshold. A tire skid mark began near the runway centerline, approximately 150 feet prior to the airplane stopping point. The first 15 to 20 feet of the skid mark was light and was oriented approximately parallel to the runway. The mark then began to turn to the left, and became darker. About halfway (laterally) between the initiation point and the runway edge, the skid mark became very pronounced, and then sequentially exhibited a cusp to the right, an interruption, and an 'S' bend. It then continued nearly straight, oriented about 45 degrees to the runway edge, before curving right, and terminated about 2 feet prior to the runway edge. The soil was disturbed between the skid mark and the airplane just beyond it. The alignment of the skid mark and airplane was consistent with it having been made by the right main tire.
The airplane sustained damage to both wings, vertical stabilizer and rudder, cowl, firewall, engine mounts, and propeller. There was no fire, and there was negligible leakage of fuel or other fluids. ADDITIONAL INFORMATIONAirplane Examination
A few days after the accident, an FAA airworthiness inspector examined the recovered airplane. His examination did not reveal any apparent anomalies or pre-impact deficiencies. About one month later, the FAA inspector and the NTSB investigator examined the airplane in detail, in a hangar of the L71 facility that the pilot was planning to visit for his pre-accident sheet metal repair cost estimate.
Some interior and exterior components and panels were removed to enable access to the entire rudder/tailwheel control system. A 'Leatherman' type multi-tool (in its case) was found on the right cockpit floor, forward of the copilot's right rudder pedal. When found, it was not in a position/location that impeded rudder pedal travel, but its original (pre-accident) position/location was not able to be determined. The pilot/owner identified the tool as his. He noted that many cockpit/cabin items were displaced during the accident, and that at least one item had not been located. That item was not recovered by the investigators during their examination.
All control cables were found to be properly routed, and no components (pulleys, bellcranks, etc) displayed any unusual wear, corrosion, damage, or other anomalies that could be associated with previous or potential control interference.
Because the rudder & vertical stabilizer damage precluded full and free travel of the rudder, the deformed sections were cut away just below the upper rudder hinge, in order to free the rudder for normal travel for the examination. The aft fuselage was hoisted to lift the tailwheel off the ground. The bottom end of the rudder and the tailwheel appeared centered/neutral when the rudder pedals were set to the 'neutral' (left and right pedals 'even' with one another) position; this was confirmed for both the pilot's & copilot's pedal sets.
Both sets of cockpit rudder pedals were then exercised to their travel limits, and the system operation, and rudder and tailwheel deflections, were noted. The rudder and tailwheel responded similarly, irrespective of which pedal set (pilot vs copilot) was exercised. The rudder travel was bounded in both directions by the rudder stops, which were properly safetied. No binding, unusual noises, or other anomalies were noted when the pedals were exercised. Cable tensions were measured, and found to be within the proper range.
Rudder deflections (from neutral/0º) in the plane parallel to the airplane longitudinal and lateral axes were measured to be as follows:
- Left: 13º
- Right: 16º
The tailwheel was a Scott fully castering model, capable of swiveling 360º in either direction, with a centering detent. All cables, springs, and other components were properly routed, connected, and safetied. Manual manipulation of the tailwheel indicated that it operated normally.
Refer to the NTSB public docket for this accident for additional examination details.
Cessna Rudder Travel Limit Values
Per the Cessna Maintenance Manual (MM), the proper rudder travel limits, measured in the plane parallel to the airplane "waterline" and lateral axes, were 24º either side of the neutral/0º position. Those same values were published in the FAA Type Certificate Data Sheet (TCDS) for the airplane.
Previous Airplane Condition and Maintenance
The pilot arrived at the examination hangar towards the end of the examination. After the examination was completed, as the investigators were preparing to depart, the pilot mentioned that the reason that he had flown the airplane to L71 was to get a cost estimate to have his rudder "re-skinned." He explained that the re-skinning was intended to correct an improper top-to-bottom curvature (bowing) of the rudder, which was apparently the result of a previous accident.
The pilot did not know whether the rudder was deformed during that accident, or as a result of improper repair. He discovered the bowing problem shortly before the subject...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR16LA108