N1551C

Substantial
None

BEECH C90AS/N: LJ-1365

Accident Details

Date
Tuesday, February 14, 2017
NTSB Number
CEN17LA121
Location
Rattan, OK
Event ID
20170307X03418
Coordinates
34.238609, -95.253890
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The loss of electrical power due to the pilot’s inadvertent selection of the engine start switches and the subsequent fuel exhaustion to the left engine as the pilot attempted to locate visual meteorological conditions. Contributing to the accident were the pilot’s failure to ensure adequate fuel reserves on board for the flight in instrument meteorological conditions and the miscommunication between the pilot and medical crewmembers.

Aircraft Information

Registration
N1551C
Make
BEECH
Serial Number
LJ-1365
Engine Type
Turbo-shaft
Year Built
1994
Model / ICAO
C90ABE9L
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
EAGLEMED LLC
Address
6601 W PUEBLO DR
Status
Deregistered
City
WICHITA
State / Zip Code
KS 67209-2926
Country
United States

Analysis

On February 14, 2017, about 1145 central standard time, a Beech C90A twin-engine airplane, N1551C, was substantially damaged during a precautionary landing following a loss of power on one engine near Rattan, Oklahoma. The pilot and two medical crew members on board were not injured. The airplane was registered to and operated by EagleMed LLC under the provisions of Title 14 Code of Federal Regulations Part 135 air medical flight. The pilot stated that the engine start and airplane power-up were normal. The engine ice vanes were lowered, and the de-icing system was activated as required for ground operations. The ice vanes were subsequently raised before takeoff. Takeoff and climb out were routine, and he subsequently leveled off the airplane at 7,000 ft. mean sea level (msl). The air traffic controller informed him of "heavy rain showers" near the destination airport and he "put the ice vanes down." Shortly afterward, the airplane experienced two "quick" electrical power fluctuation; "everything went away and then came back." "Seconds later the entire [electrical] system failed." Due to the associated loss of navigation capability while operating in instrument meteorological conditions, the pilot set a general course for better weather conditions based upon the preflight weather briefing.

During the attempt to find a suitable hole in the clouds to descend through under visual conditions, the left engine lost power. The pilot ultimately located a field through the cloud cover and executed a single engine precautionary landing. The nose landing gear collapsed, and the airplane sustained substantial damage to the right engine mount and firewall.

A postaccident examination was conducted by Federal Aviation Administration inspectors and operator personnel. The left propeller blades were bent aft and did not exhibit any curling of the blades. The right propeller blades were curled in the direction of rotation. The left- and right-wing fuel tanks did not contain any visible fuel. The left nacelle fuel tank did not contain any visible fuel. The right nacelle fuel tank appeared to contain about one quart of fuel. The three-position Ignition and Engine Start/Starter Only switches on the cockpit instrument panel were in the ON position. The Engine Anti-Ice switches were in the ON position. The cabin medical bed electrical switches corresponding to the inverter and accessories were in the ON position; the remaining medical bed switches were OFF. A postrecovery examination was conducted by the NTSB investigator-in-charge and operator personnel. No anomalies consistent with an in-flight electrical system malfunction were observed. When the airplane battery was initially checked during the exam the voltmeter indicated 10.7 volts; the battery was charged and appeared to function normally thereafter.

The operator reported that 253 gallons (1,720 lbs.) of fuel were onboard at takeoff and the airplane gross weight was 7,838 lbs. The accident flight duration was 3.65 hrs. Airplane performance data indicated that at maximum cruise power, the expected fuel flow would be about 632 lbs./hr., resulting in an endurance of approximately 2.7 hrs. At maximum range power, the expected fuel consumption was about 406 lbs./hr., resulting in an endurance of approximately 4.2 hrs.

Both the pilot and medical crew described a lack of communication and coordination among crew members. The pilot reported that the medical crew became apprehensive as the emergency transpired. On three occasions, as the pilot maneuvered the airplane attempting to locate a hole in the clouds to descend, the medical crew member in the co-pilot seat grabbed the control wheel to keep the pilot from banking the airplane. He subsequently relinquished the control wheel as directed by the pilot. The medical crew attempted to locate the airplane by using cellphones to coordinate with the operator's operations center or by using the cellphone GPS capability. However, these efforts resulted in multiple course adjustments and ultimately failed to encounter visual meteorological conditions before fuel exhaustion on the left engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA121