N714DW

Substantial
None

CESSNA 150MS/N: 15079105

Accident Details

Date
Tuesday, May 9, 2017
NTSB Number
ERA17LA176
Location
Homerville, GA
Event ID
20170510X11422
Coordinates
31.053333, -82.771110
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power due to inadequate maintenance and inspection of the engine, which resulted in a fatigue crack and subsequent failure of the No. 4 cylinder.

Aircraft Information

Registration
Make
CESSNA
Serial Number
15079105
Engine Type
4-cycle
Model / ICAO
150MC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
150M

Registered Owner (Current)

Name
ERDMAN DANIEL J
Address
1934 PROSPECT AVE
City
HERMOSA BEACH
State / Zip Code
CA 90254-3342
Country
United States

Analysis

On May 9, 2017, about 1525 eastern daylight time, a Cessna 150M, N716DW, was substantially damaged when it was involved in an accident near Homerville, Georgia. The pilot was uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he was in cruise flight at 3,000 ft mean sea level when he heard an unusual sound come from the engine and the engine power began to decrease to 1,500 rpm. The pilot turned the carburetor heat on, but power was not restored. He then checked the positions of the fuel selector and the engine primer. Light smoke began to enter the cockpit, and at the same time, a small piece of debris struck the windshield. The pilot declared an emergency with air traffic control, established the airplane at its best glide airspeed, and began looking for a suitable forced landing area.

As he descended the airplane toward the forced landing site, the pilot turned off electrical power. The main landing gear touched down first; however, the surface of the field was soft and rough, and the airplane nosed over and came to rest inverted.

Examination of the engine revealed that the barrel of the No. 4 cylinder separated at a point halfway along the length of the barrel and the No. 4 piston displayed heavy impact damage. The No. 4 connecting rod was bent, and the No. 4 piston pin was missing.

Examination of the components of the No. 4 cylinder by the NTSB Materials Laboratory revealed that the connecting rod, cap, and bolts were all intact, with no fractures; however, the connecting rod body was deflected along the web near the piston pin bore. The sides of the rod exhibited scraping or gouging damage, and the pin bore of the connecting rod was deformed, consistent with elongation along the length of the rod.

The crankshaft bearing surfaces were intact and exhibited minimal wear. Much of the piston exhibited severe deformation and material loss. The fracture surfaces on the underside of the piston were heavily damaged due to post-fracture impact and corrosion damage. The visible fracture features were consistent with overstress, with the fracture originating about the pin hole bore of the piston. The cylinder had fractured about the compression wall at the 10th cooling fin valley when counted from the larger main body cooling fins of the cylinder head. Several of the fin flange surfaces exhibited small circular features consistent with pitting.

The fracture located on the head side and the piston, or open, side of the cylinder halves were relatively flat and exhibited a reflective luster. Much of the fracture surface was damaged or entirely obliterated by post-fracture smearing or contact.

Closer examination of the head side fracture surface revealed that a portion exhibited crack arrest marks consistent with fatigue cracking. The crack arrest features were present along approximately 30% of the fracture surface circumference and propagated around the cylinder cross section from a singular point. The crack initiation site was located on the exterior surface of the cylinder fin valley. An initial thumbnail crack was present adjacent to the crack initiation site, with radial marks and crack arrest marks propagating outward.

The cylinder fracture surfaces were examined using a scanning electron microscope. An area of undamaged fracture surfaces near the end of the progressive cracking area displayed crack arrest marks and radial lines consistent with the crack propagation direction. Inside this region, fatigue striations were present, consistent with fatigue crack propagation. Outside the fatigue crack, dimple rupture was observed, consistent with subsequent overstress fracture.

Multiple corrosion pits were present at the fatigue crack initiation site. The pits contained non-conductive (non-metallic) compounds consistent with an iron oxide, containing detectable levels of sodium, magnesium, phosphorus, potassium, sulfur, and calcium. These elements were not present in the bulk of the materials. The chemical composition was consistent with an alloy steel.

A portion of the cylinder and fins near the fracture surface was sectioned, mounted, and polished for metallographic examination. Of note were features present along the adjacent cooling fin valleys where corrosion pits were present on the surface, with non-metallic compounds contained within. These corrosion pits were found on much of the surfaces examined in the cross-section. The composition of these compounds, as examined using energy dispersive x-ray spectroscopy, was consistent with that of the iron oxide compounds observed on the corrosion pits at the fatigue crack initiation site on the fracture surface.

Surface corrosion was present at all the examined fin valleys. The chemical composition of these compounds was consistent with that of the corrosion pit compounds, and further examination revealed that the surface corrosion compounds were cracked and discontinuous. The underlying interface with the base metal was also tortuous in morphology, consistent with widespread pitting corrosion.

Continental Motors Service Information Letter 98-9C stated that the time between overhaul (TBO) for the O-200-A engine was 2,000 hours of operation or 12-years (whichever occurred first), and that an engine’s published TBO does not mean that every engine will operate the number of hours or years listed without requiring component replacements and/or unscheduled maintenance events. Noncompliance with instructions for continued airworthiness, operational and/or environmental factors may necessitate repair or replacement of the engine, engine components and accessories earlier than the published TBO.

According to FAA and maintenance records, the engine was manufactured on April 22, 1970. The engine received a complete overhaul on August 9, 1996. The engine was "top overhauled" with four new ECI cylinders on May 15, 2008.

The airplane's most recent annual inspection was completed on May 3, 2017. At the time of the accident, the airplane had accrued about 7,341.7 total hours of operation, and the engine had accrued about 2,249.3 total hours since the 1996 overhaul.

A nearly identical cylinder failure was documented in 2016 (NTSB Case No. CEN16LA306). Examination of that engine revealed that the No. 2 cylinder was completely separated between the flange and the head as the result of a fatigue crack that initiated at a cooling fin valley on the exterior surface. The fatigue crack grew around 40% of the circumference of the cylinder, and overstress led to the eventual cylinder fracture. A metallographic cross-section of the cylinder revealed corrosion pits under the paint and primer.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA17LA176