Accident Details
Probable Cause and Findings
The pilot's failure to maintain adequate airspeed, properly correct for left yaw, and his exceedance of the airplane's critical angle of attack during initial climb, which resulted in an aerodynamic stall and subsequent uncontrolled descent into water.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn June 3, 2017, about 1417 Atlantic standard time, a Piper PA-23-250, N21WW, impacted water and a reef shortly after takeoff from Luis Munoz Marin International Airport (TJSJ), San Juan, Puerto Rico. The commercial pilot sustained minor injuries, two passengers were seriously injured, and one passenger was fatally injured. The airplane was destroyed. The flight was being operated by Air America, Inc., as a Title 14 Code of Federal Regulations Part 135 on-demand air taxi flight. Visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the planned flight to Benjamin Rivera Noriega Airport (TJCP), Isla de Culebra, Puerto Rico.
According to air traffic control (ATC) information provided by the Federal Aviation Administration (FAA), the flight was cleared for an intersection takeoff on runway 8 from taxiway S5. Runway 8 was 10,400 ft long, and the intersection takeoff at S5 allowed about half of the runway length for takeoff. At 1414:09, the pilot contacted ATC and stated that he was ready for takeoff. The tower controller replied that there was about 30 seconds left of a wake turbulence delay due to an Embraer 190 that had departed about 2 minutes 30 seconds earlier. The pilot waived the delay, and the tower controller cleared the flight for takeoff at 1414:26. At 1416:33, the tower controller instructed the pilot to contact departure control; however, the pilot stated that he was "unable" and was returning to the airport. At 1416:46, the pilot stated, "we are trying hard we lost power on an engine we're trying to go back." The controller asked what engine, and the pilot replied, "we… [lost] an engine." No further communications were received from the pilot.
Review of radar data revealed that, at 1415:52, the airplane was near the departure end of the runway, indicating an altitude of 100 ft. The last radar target was recorded at 1416:16, about 1,000 ft beyond the departure end of the runway, indicating an altitude of 0 feet (about 100 ft agl). Review of airport surveillance video revealed that the airplane had lifted off the runway by about 1415:40 and had climbed to between about 100 and 150 ft agl, out of ground effect, as it passed over the departure end of the runway at 1416:01. The airplane remained in a nose-up attitude and began to descend; it then entered a shallow left turn at 1416:17. The airplane continued turning left at a low altitude to a position consistent with the left downwind leg of the airport traffic pattern and then disappeared from the camera's view at 1416:43. The airplane reappeared in the camera's view as it impacted water about .75 mile abeam the departure end of runway 8 at 1417:07.
According to the pilot's written statement and recorded interview, after he completed a preflight inspection, the passengers walked toward the airplane. The pilot then completed a final walkaround and visually checked the fuel in the fuel tanks. After the baggage was loaded and the passengers boarded the airplane, the pilot performed a safety/emergency briefing and started the engines. He received instructions from ATC to taxi to runway 8 via N taxiway and to hold short of the runway at S5. The pilot performed a run-up using the checklist, and everything was within acceptable parameters.
After receiving clearance for takeoff from ATC, the pilot performed a takeoff roll and rotated the airplane at 85 knots. About 100 ft agl, he retracted the landing gear and noted that the airplane did not seem to be climbing or accelerating beyond 85 to 90 knots. He verified that the magnetos and fuel pumps were on and that the throttle, mixture, and propeller levers were in the "full forward" position. He also noted that all the engine instruments were in the green arc normal operating range. The airplane then yawed left, and the pilot noticed that the left engine rpm was less than the right, but that it remained in the green arc. The pilot subsequently turned left with the yaw to return to the airport, but the airplane was unable to maintain altitude. He then attempted to avoid a populated beach and ditched in shallow water. The pilot did not remember how he exited the airplane, but recalled that his face burned when he swam to the water's surface because of a fire. He tried two more times to reach the water's surface far enough away from the fire. He then saw two of the three passengers and attempted to swim back for the third passenger, but was in shock and had ingested too much water. A person on a paddle board then pulled the pilot from the water.
During a postaccident interview with two FAA inspectors, the front seat passenger stated that he was not a pilot, but that he was familiar with airplanes because he was an aerospace engineer and had spent some time in a Boeing 757 simulator with a friend. He stated that the pilot did not provide a safety briefing and that, instead, he (the front seat passenger) instructed the other passengers (minors) to fasten their seatbelts, and he fastened his seatbelt. As the airplane approached the runway, the pilot secured the door and started the takeoff process without reading any checklist. The airplane initially gained some altitude, but it then yawed left. The front seat passenger then noticed that the pilot did not correct the yaw and let the airplane turn perpendicular to the wind, at which point, he mentally questioned the pilot's competency and felt compelled to take the controls, but he did not touch anything. The airplane lost altitude and flew under a tree line while remaining in a left banking turn. The pilot then moved the yoke abruptly right, and the airplane collided with the water.
The front seat passenger reported that the pilot egressed first, but he did not recall how because the door was on the passenger's side of the airplane. The front seat passenger then egressed, followed by one other passenger. The third passenger did not egress, and the front seat passenger tried to go back toward the airplane, but the fire was too intense, and he was badly burned. The front seat passenger added that the sound of the engines did not change during the flight and that he noted no smoke or fuel odor. PERSONNEL INFORMATIONThe pilot held a commercial pilot certificate with ratings for airplane single-engine land, airplane multiengine land, and instrument airplane. He also held a flight instructor certificate with ratings for airplane single-engine and airplane multiengine. The pilot's most recent FAA first-class medical certificate was issued on December 14, 2016. The pilot reported a total flight experience of about 1,200 hours, about 200 hours of which were in multiengine airplanes and about 20 hours of which were in the accident airplane make and model.
Review of company records revealed that the pilot was hired in December 2016 and completed ground and flight training. At the time of his hire, he reported a total flight experience of 900 hours, 110 hours of which were in multiengine airplanes. From December 2016 through May 2017, the pilot flew about 220 hours in a Britten-Norman BN-2A-21 Islander, which could carry up to nine passengers and was equipped with two 300-horsepower Lycoming engines. The pilot completed training in the accident airplane make and model on May 25, 2017. He had accumulated about 20 hours in it during the 6 months before the accident. At the time of the accident, the last recorded entry in the pilot's logbook was dated February 28, 2017. At that time, the logbook indicated that the pilot had accumulated a total flight experience of about 933 hours, 234 hours of which were in multiengine airplanes.
Review of the pilot's FAA records revealed that he received a Notice of Disapproval of Application for a private pilot certificate on November 8, 2014. The pilot subsequently obtained his private pilot certificate on November 12, 2014. The pilot then obtained a multiengine rating during his first attempt on December 4, 2014. He received another Notice of Disapproval of Application for an instrument rating on January 30, 2015. The notice included comments that, upon reapplication, the pilot would be reexamined on preflight preparation and preflight procedures. He subsequently obtained an instrument rating on February 6, 2015. The pilot obtained a commercial pilot license (single-engine land) during his first attempt on March 18, 2015. He also obtained a commercial pilot certificate (multiengine land and instrument airplane) during his first attempt on April 11, 2015.
The pilot received another Notice of Disapproval of Application for a flight instructor certificate (multiengine rating) on June 16, 2015. The notice included comments that the pilot needed to review and understand the airplane's systems. The pilot subsequently obtained his flight instructor certificate with a multiengine rating on July 7, 2015. At that time, the pilot reported a total flight experience of 221 hours, 96.9 hours of which were in multiengine airplanes. The pilot received another Notice of Disapproval of Application for a flight instructor certificate (single-engine rating) on July 14, 2015. The notice included comments that the pilot needed more training teaching takeoffs and landings. The pilot subsequently obtained his flight instructor certificate with a single-engine rating on July 22, 2015. AIRCRAFT INFORMATIONThe six-seat, low-wing, tricycle-retractable-gear airplane was manufactured in 1975. It was powered by two Lycoming IO-540, 250-horsepower engines, each equipped with a Hartzell controllable pitch full-feathering propeller. According to maintenance records, the airplane's most recent annual inspection was completed on November 16, 2016. At that time, the airframe had accumulated 9,087.3 total hours of operation, and the engines had accumulated 695.3 hours since major overhaul. The airplane had flown about 95 hours from the time of that inspection until the accident.
Review of the airspeed indicator ...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA17FA195