N3047J

Substantial
None

CESSNA A188BS/N: 18803596T

Accident Details

Date
Friday, August 4, 2017
NTSB Number
CEN17LA303
Location
Marshall, MO
Event ID
20170806X13056
Coordinates
39.095554, -93.202774
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inability to accurately monitor the airplane's airspeed after takeoff due to an inoperative airspeed indicator, which resulted in the pilot's failure to maintain adequate airspeed and his exceedance of the airplane's critical angle of attack and the subsequent aerodynamic stall/mush and degraded climb performance.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18803596T
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
A188BC188
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
A188B

Registered Owner (Current)

Name
DARTER LLOYD R
Address
8699 CANARY LN
City
MOUNTAIN GROVE
State / Zip Code
MO 65711-2563
Country
United States

Analysis

***This report was modified on March 8, 2018. Please see the docket for this accident to view the original report.***

On August 4, 2017, about 0900 central daylight time, a Cessna A188B airplane, N3047J, was substantially damaged when it settled into a bean field after takeoff from runway 18 (5,006 feet by 75 feet, concrete) at the Marshall Memorial Municipal Airport (MHL), Marshall, Missouri. The pilot was not injured. The airplane was registered to and operated by private individuals as a 14 Code of Federal Regulations Part 137 flight. Visual meteorological conditions prevailed. The flight was not operated on a flight plan. The local aerial application flight was originating at the time of the accident.

The pilot stated that the airplane was loaded with about 120 gallons of fertilizer and 54 gallons of fuel at the time of the accident takeoff. The pretakeoff run-up was normal. After takeoff, he reduced engine power for climb. When he did so, the engine "surged." He responded by increasing the throttle "a little," but the engine "surged" again. He subsequently applied full throttle, but was unable to maintain a positive rate of climb. The airplane settled into a bean field and encountered a fence before coming to rest in the adjoining corn field.

The pilot informed a Federal Aviation Administration (FAA) inspector that the airplane seemed to be "sagging" after takeoff. The engine indications appeared to be normal before the accident. The airplane had a full load of fertilizer and fuel at the time of the accident takeoff. The pilot also informed the inspector that the airspeed indicator had been inoperative for some time.

A postaccident engine examination conducted by FAA inspectors did not reveal any anomalies consistent with a preimpact loss of engine power. The wing flaps were positioned at 20 degrees deflection at the time of the exam.

The airplane flight manual noted that the recommended takeoff wing flap setting for restricted category airplanes was 10 degrees. The approved takeoff range for normal category airplanes was 0 to 20 degrees. The information manual indicated that optimum takeoff performance at heavy weights is obtained using 10 degrees wing flaps.

FAA regulations (14 CFR 91.205) require an operational airspeed indicator for civil aircraft operating under a standard airworthiness certificate. The accident airplane was operating under a restricted category airworthiness certificate and was not required to comply with that regulation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA303