N91904

Substantial
None

EMERSON KitfoxS/N: 61

Accident Details

Date
Sunday, September 24, 2017
NTSB Number
CEN17LA366
Location
Waller, TX
Event ID
20170926X85855
Coordinates
29.984722, -95.931114
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power for reasons that could not be determined based on the available information.

Aircraft Information

Registration
N91904
Make
EMERSON
Serial Number
61
Engine Type
Reciprocating
Model / ICAO
KitfoxBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
RAMSEY BRADY D
Address
119 BEAVERS RD
Status
Deregistered
City
ELM MOTT
State / Zip Code
TX 76640-3510
Country
United States

Analysis

On September 24, 2017, about 1700 central daylight time, an experimental, amateur-built Emerson Kitfox airplane, N91904, collided with terrain following a loss of engine power after takeoff from the Skydive Houston Airport (37XA), Waller, Texas. The pilot was not injured, and the airplane sustained substantial damage. The airplane was registered to a private individual and was being operated by the pilot as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions existed near the accident site at the time of the flight, and a flight plan had not been filed. The flight was departing 37XA on a local flight.

The pilot reported he did a preflight and engine run-up and it appeared the airplane was operating normally. He decided to takeoff and fly around the traffic pattern. The airplane climbed to 300 to 400 ft above ground level when there was a partial loss of engine power. He stated that the engine continued to operate but did not develop enough power to sustain flight. The pilot attempted to land in a field near a residential area, and the airplane impacted a fence which resulted in substantial damage to the wings and fuselage. The pilot purchased the airplane in October 28, 2016, and the fuel in the airplane had not been changed since at least October 2016.

The airplane was manufactured in 2001 but had never received an airworthiness certificate. The pilot did not have a current medical certificate.

The wreckage was examined by a FAA operations inspector who performed a limited inspection of the airplane. The inspector determined there was fuel at the scene and there was no evidence of water in the fuel. No further examination into the cause of the loss of engine power was conducted.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA366