N714TD

Substantial
Minor

CESSNA 152S/N: 15279413

Accident Details

Date
Sunday, December 3, 2017
NTSB Number
WPR18LA042
Location
Everett, WA
Event ID
20171204X72456
Coordinates
47.907600, -122.280900
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The flight instructor’s inadequate preflight inspection, during which he failed to ensure that water was sufficiently drained from the fuel system, which resulted in total loss of engine power and a subsequent forced landing and impact with objects.

Aircraft Information

Registration
N714TD
Make
CESSNA
Serial Number
15279413
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
152C152
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MORCOM AVIATION SERVICES INC
Address
10100 30TH AVE W STE C51
Status
Deregistered
City
EVERETT
State / Zip Code
WA 98204-1308
Country
United States

Analysis

On December 3, 2017, about 1325 Pacific standard time, a Cessna 152 airplane, N714TD, was substantially damaged when it was involved in an accident near Everett, Washington. The flight instructor and student pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the flight instructor, after conducting a local, instructional flight, he and the student pilot returned to the airport to practice touch-and-go landings. After successfully completing one touch-and-go landing, they switched to another runway. During the approach, the airplane was high on the glidepath, and the student subsequently initiated a go-around. The instructor stated that, during the go-around, when the airplane was about 150 ft above ground level, the engine “sputtered” and then lost all power. Realizing the airplane would not be able to reach the runway, they chose to conduct a forced landing in a nearby field, during which the left wing stuck a utility pole, and the right wing struck a tree.

Postaccident examination of the airplane revealed that the wings had sustained substantial damage. When the fuel tank sumps and strainer were drained, a large amount of water was observed in the fuel. During an engine test run, the engine had difficulty starting. After the carburetor was replaced, the engine started with some hesitation but then ran smoothly at various power settings. Examination of the carburetor revealed no evidence of any preaccident mechanical malfunctions or failures that would have precluded normal operation, and no debris or contaminants were found.

The Pilot’s Operating Handbook, Section 4, “Normal Procedures,” “Preflight Inspection,” stated, in part, the following:

Before the first flight of the day and after each refueling drain a small quantity of fuel from the fuel tank sump quick-drain valve to check for water…pull out [the] strainer drain knob for about four seconds to clear fuel strainer of possible water and sediment. Check strainer drain closed. If water is observed, the fuel system may contain additional water, and further draining of the system at the strainer, fuel tank sumps, and fuel line drain plug will be necessary.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR18LA042