N5382A

Substantial
None

CESSNA T210S/N: 21063404

Accident Details

Date
Tuesday, March 13, 2018
NTSB Number
ERA18LA103
Location
Orlando, FL
Event ID
20180313X72120
Coordinates
28.289722, -81.436943
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The improper adjustment of the fuel pump by maintenance personnel, which resulted in an overly rich fuel/air mixture and a total loss of engine power.

Aircraft Information

Registration
N5382A
Make
CESSNA
Serial Number
21063404
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
T210T210
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
3011 W BUCKEYE RD
Status
Deregistered
City
PHOENIX
State / Zip Code
AZ 85009-5734
Country
United States

Analysis

On March 13, 2018, about 1330 eastern daylight time, a Cessna T210N, N5382A, was substantially damaged when it was involved in an accident near Orlando, Florida. The commercial pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he and a coworker were conducting routine test flights with new camera equipment that had just been installed on the airplane. On the morning of the accident, the pilot performed a two-hour test flight with no issues. After starting the engine and waiting about 5 minutes to allow the camera system to boot up, the pilot taxied to the runway and was cleared for takeoff. As the airplane climbed, he felt there was something wrong with the engine, although it continued to produce power. He checked all the instruments and gauges and did not see any abnormalities. When the airplane reached cruise altitude, the pilot reduced power and the engine "quit." The pilot notified air traffic control of the engine failure and performed a forced landing on a road.

Examination of the airplane by a Federal Aviation Administration inspector revealed that the empennage was separated from the fuselage. Both wings were buckled, and both wing assemblies were leaking fuel.

The engine was removed and sent to the manufacturer for further examination and testing. After an examination, the engine was prepared and placed in an engine test cell. The engine ran normally up to about 2,100 rpm, then emitted black smoke from the exhaust and began to lose power when the throttle was increased, consistent with an overly rich fuel/air mixture. The fuel pump was leaned, and further test runs were completed with no anomalies. The unmetered pressure was at or slightly above the maximum pressure for full throttle. Upon completion of the standard run, the fuel pump was set back to the as-received setting and exhibited the same loss of power demonstrated during the first test.

The throttle body and fuel pump were bench tested and both units failed to meet production standards.

A review of the maintenance logbook entries revealed that on July 25, 2016, a fuel system adjustment was performed at a tachometer time of 9,854.4 hours. As of the last annual inspection on February 25, 2018, the engine had accumulated a total of 455.6 hours.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA18LA103