N78417

Substantial
None

Cessna A188S/N: 18801952T

Accident Details

Date
Wednesday, August 22, 2018
NTSB Number
CEN18LA350
Location
Atchison, KS
Event ID
20180825X12218
Coordinates
39.575832, -95.181114
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The partial loss of engine power for reasons that could not be determined during the postaccident examination.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18801952T
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
A188C188
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
A188B

Registered Owner (Current)

Name
MCELWAIN RUSSELL D
Address
11599 286TH RD
City
LANCASTER
State / Zip Code
KS 66041-9138
Country
United States

Analysis

On August 22, 2018, about 1600 central daylight time, a Cessna A188 airplane, N78417, impacted terrain after departing the Amelia Earhart Airport (K59), Atchison, Kansas. The pilot was not injured, and the airplane was substantially damaged during the accident. The airplane was registered to a private individual and operated by McElwain Sprayers, LLC under the provisions of Title 14 Code of Federal Regulations Part 137 as an agricultural flight. Visual meteorological conditions prevailed at the time.

The pilot reported he topped off with fuel in the morning and had flown two previous loads. On the third takeoff, as the airplane was 70 to 75 mph, the airplane "would not come off the ground." He said that the mixture was full rich, and the propeller and throttle controls were full forward. He felt he could not stop on the remaining runway, so he dumped the load, in order to reduce the airplane's weight, in an attempt to get airborne. However, the airplane did not get airborne, and the airplane impacted terrain just beyond the runway. After the airplane came to rest, the pilot said he pulled the mixture control back, turned the magnetos and battery off, and exited the airplane.

The airplane's owner saw the attempted takeoff. He reported that the engine puffed black smoke during the takeoff run. He added that the fuel servo provided a mixture that was too rich, so on the ground the pilots would reduce the mixture, and then use a full rich mixture for takeoff. After the accident, he said the mixture control was back two inches, which was too far.

The responding Federal Aviator Inspector noted substantial damage to the fuselage and wings. A visual inspection of the engine did not find any abnormalities.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA350