N65MY

Destroyed
Fatal

Beech 60S/N: P-314

Accident Details

Date
Friday, April 19, 2019
NTSB Number
WPR19FA115
Location
Fullerton, CA
Event ID
20190418X14517
Coordinates
33.871387, -117.981390
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s use of an unapproved elevator control lock device, and his failure to remove that device and correctly position the elevator before flight, which resulted in a loss of control during takeoff. Contributing to the accident was his failure to perform a preflight inspection and control check, likely in part because of distractions before boarding and his late departure time.

Aircraft Information

Registration
N65MY
Make
BEECH
Serial Number
P-314
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
KMA TECHNOLOGY SOLUTIONS LLC
Address
PO BOX 1840
Status
Deregistered
City
HELENA
State / Zip Code
MT 59624-1840
Country
United States

Analysis

HISTORY OF FLIGHTOn April 18, 2019, about 1951 Pacific daylight time, a Beech B60, N65MY, was destroyed when it was involved in an accident near Fullerton, California. The private pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot’s relatives, he typically flew the accident airplane from Heber City, Utah, to Fullerton on Monday mornings and returned Thursday nights. If the weather was bad, he would take a commercial flight.

The accident sequence was captured by a series of video surveillance cameras located at multiple vantage points on the airport property. Review of the video data revealed that the pilot boarded the airplane at his hangar about 1928. He started the engines and taxied about 500 ft to the runup area at the east end of the airport, where the airplane remained for the next 11 1/2 minutes. During that time, the pilot was provided his instrument flight rules (IFR) clearance by the tower controller. The airplane then taxied to the hold short line on taxiway A at the approach end of runway 24.

After the pilot was given the takeoff clearance, the airplane began the takeoff roll. The airplane was airborne after traveling about 1,300 ft down the runway, and about 2 seconds after rotation, it began to roll to the left. Three seconds later, the airplane had reached an altitude of about 80 ft above ground level and was in a 90° left bank (figure 1). The nose then dropped as the airplane rolled inverted and struck the southern side of taxiway E in a right-wing-low, nose-down attitude.

Figure 1. Composite video surveillance image of takeoff as viewed from the north.

PERSONNEL INFORMATIONThe pilot held a private pilot certificate issued in May 2011. He attained his instrument and multiengine ratings in January 2012 and January 2014 respectively. His logbooks indicated 35.6 hours of pilot-in-command night flight experience.

Before the pilot began flying the accident airplane in October 2017, he had 2 hours of flight experience in the airplane type. Of the 101 hours of flight time that he accrued between October 2017 and the accident, 87 hours were flown in the accident airplane.

METEOROLOGICAL INFORMATIONOn the day of the accident, sunset occurred in Fullerton at 1825, and clear skies with light wind conditions were forecast for Heber City throughout the evening.

WRECKAGE AND IMPACT INFORMATIONAn on-site examination showed that the first identified point of impact was located on taxiway E about 100 ft south of the runway 24 centerline. A set of four impact gouges were oriented diagonally across the centerline and spaced about 8 inches apart and matched the approximate dimension of the right propeller blades; a similar set of gouges were on the pavement about 18 ft to the southwest. Fragmented sections of the outboard right wing were distributed around the impact point and on the adjacent runway surface.

The main wreckage came to rest on taxiway A, about 100 ft beyond the second set of gouges. The main wreckage was comprised of the pressurized section of the cabin, both engines, the left wing, and the tail section, all of which sustained extensive thermal damage. The entire tail structure aft of the pressure bulkhead was thermally consumed, and only ash remnants of the vertical and horizontal stabilizer and flight control surfaces remained. The landing gear actuator was fully extended. Although the left flap actuator was partially consumed, the right flap actuator displayed an extension which corresponded with the flaps set to about 10°. Examination of video footage also confirmed that the flaps were extended as the airplane taxied onto the runway and that the landing gear was in the down position at the time of impact.

The cockpit instruments and circuit breakers were all fire damaged, which precluded an accurate assessment of their readings and positions. The throttle and propeller engine controls were in the full forward position. The pilot seat, which was equipped with forward and aft seat stops, had detached but did not appear to be positioned close to the aft limits of the seat rails at impact.

There were no tools or foreign objects present in the footwell area enclosing the aileron pulleys and servo. Although the flight control systems sustained varying degrees of impact and thermal damage, control continuity was confirmed between the cabin controls and the respective control surfaces.

The elevator trim actuator was in a 5° tab down position, and the aileron trim actuator was in a 1° tab up position. Both fuel selector valves were fire damaged but appeared set to the “ON” position.

Most of the right wing’s structure was consumed, exposing the landing gear actuators, engine control cables, and fuel selector valve. The left wing remained attached to the fuselage; its main spar was intact along its full length, and the aft spar and trailing skins were mostly consumed by fire.

On-site examination showed that both propeller hub assemblies had separated from their respective engines at the crankshaft and were located on the grass adjacent to the impact point. Postaccident examination of the propellers revealed that multiple blades of both propellers exhibited similar curl and twist damage opposite the direction of rotation as well as leading edge gouges and scoring. The symmetry of damage between both propeller assemblies was consistent with both engines producing equal amounts of power at impact.

Postaccident engine examination of both engines revealed varying degrees of thermal and impact damage but no evidence of catastrophic internal failure. Drive train continuity was confirmed, and both the fuel and oil filters were free of debris.

MEDICAL AND PATHOLOGICAL INFORMATIONAccording to the autopsy performed by the Orange County Sheriff-Coroner, the cause of death was multiple traumatic injuries with a finding of hypertrophic cardiomegaly (enlarged heart), but otherwise no natural disease was present.

Toxicology testing performed at the Federal Aviation Administration Forensic Sciences Laboratory did not identify the presence of any tested-for drugs, ingested alcohol, or carbon monoxide.

TESTS AND RESEARCHEngine Monitor

The airplane was equipped with a G4 graphic engine monitor that was manufactured by Insight Avionics. It was configured to monitor and record cylinder head temperature (CHT), exhaust gas temperature (EGT), turbine inlet temperature (TIT), and fuel flow information for both engines.

Despite thermal damage to the engine monitor, the NTSB’s Vehicle Recorders Division extracted accident flight data from the device.

The data revealed that the EGT, CHT, and TIT values approximately matched between both engines from initial power-up through to the accident. The fuel flow for the right engine varied between about 5 and 15 gallons per hour (gph) for the first 20 minutes, which corresponded roughly from engine start to taxi. For the final 30 seconds of the accident flight, the fuel flow for the right engine increased to about 36 gph. The fuel flow for the left engine remained at 0 gph throughout the entire recording, which was inconsistent with video data and the other recorded engine parameters.

Elevator Positions

The airplane was stored in a hangar on the southeast side of the airport. A friend of the pilot who had an adjacent hangar said he was approached the evening before the accident by the pilot, who explained that one of the landing lights on the accident airplane had failed. They then worked together to replace the light bulb, and during those interactions, the pilot mentioned that one of the airplane’s circuit breakers kept tripping. The friend could not recall specifically what circuit breaker the pilot stated was tripping.

After completing the repair, they pulled the airplane out of the hangar, and the accident pilot taxied it to the fuel island. After adding fuel, they taxied to the runup area so the pilot could check the circuit breaker. He performed an engine runup, but it did not trip. The pilot’s friend was seated in the back and did not have a clear view of the instrument panel while the pilot was troubleshooting the circuit breaker issue.

As they later pushed the airplane back into the hangar, the accident pilot indicated that the elevator in the trailing edge down position typically would not clear the propeller blade of another airplane in the hangar, which the friend observed. The accident pilot then walked to the back of the airplane and appeared to move the elevator from the trailing edge down position to the trailing edge up position, where it remained, to clear the tip of the blade.

One of the surveillance cameras was positioned above the pilot’s hangar and captured the airplane as it was being moved inside that night. Review of the footage revealed that, as the airplane was first being maneuvered, the elevator was hanging at about the 15° trailing edge down position, consistent with the pilot’s friend’s observation. The following evening, as the pilot pulled the airplane back out of the hangar for the accident flight, the elevator was at about the 15° trailing edge up position such that the elevator balance weight hung below the lower skin of the horizontal stabilizer trailing edge.

The video footage also revealed that shortly after the pilot pulled the airplane out of the hangar, someone arrived at an adjacent hangar and the pilot assisted them with removing a motorbike from a trailer, talked to several individuals who had arrived, walked toward the restroom, and returned to the hangar, before immediately boarding the airplane. He did not perform a “walk around” inspection at any time after he took the airplane out of the hangar.

Review of video footage throughout the airport revealed that the elevator remained in the same trailing edge up position throughout taxi, in the runup area, and at the runway hold short line.

The video footage on the day of...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19FA115