N9WU

Substantial
Serious

JAMES Experimental CubS/N: 0003

Accident Details

Date
Thursday, June 13, 2019
NTSB Number
WPR19LA170
Location
Stanley, ID
Event ID
20190614X14254
Coordinates
44.178333, -114.891670
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

Overstress failure of the right-wing spar due to an encounter with turbulence.

Aircraft Information

Registration
Make
JAMES
Serial Number
0003
Engine Type
4-cycle
Year Built
2013
Model / ICAO
Experimental CubSBM3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
EXPERIMENTAL CUB

Registered Owner (Current)

Name
HARTMAN MATTHEW F
Address
451 PARKHILL DR
City
BILLINGS
State / Zip Code
MT 59101-0662
Country
United States

Analysis

On June 13, 2019, about 1320 mountain daylight time, an experimental, amateur-built Experimental Cub airplane, N9WU, was substantially damaged when it was involved in an accident near Stanley, Idaho. The pilot and passenger were seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that, while in the vicinity of the Sawtooth Mountain Range, the airplane encountered turbulence. As the flight continued, they encountered severe turbulence and he heard a “pop” sound. A few seconds later, the right wing began to shake "violently." He slowed the airplane and began to look for a place to land. He placed the airplane in a slight turn and the airplane encountered turbulence again. The airplane subsequently entered a spin and impacted the ground.

The accident site elevation was 7,460 ft msl and adjacent to a mountain range. There were no pilot reports of turbulence in the area.

Review of the surface analysis chart for 1200 on the day of the accident showed a low-pressure system over Idaho just south of the accident site, which was associated with a thermal low and a trough of low pressure that extended southward. Southeast of the accident site was a high-pressure system located over western Wyoming with a ridge of high pressure that extended westward into southeastern Idaho.

The closest weather reporting station was the Stanley Ranger Station, Stanley, Idaho, about 2 miles northwest of the accident site at an elevation of 6,496 ft mean sea level (msl) and a calculated density altitude of 8,844 ft at the time of the accident. The station did not report precipitation, visibility, visibility restrictions, or sky conditions. At 1348, the wind was variable at 5 knots, temperature 23°C, dew point 6°C, altimeter 30.10 inches of mercury.

A High-Resolution Rapid Refresh model sounding for the area over the accident site indicated a high probability of strong thermal activity from the surface through 7,000 ft agl.

Portions of the right-wing strut and front and rear spar were sent to the National Transportation Safety Board Materials Laboratory for examination. The forward wing spar displayed an in-plane fracture surface, consistent with a tensile overstress. The other fracture surfaces were identified as overstress and were consistent with out-of-plane plastic deformation. These fracture surfaces occur after the initial fracture or failure event and are often associated with ground impact.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19LA170