N303TL

Destroyed
Fatal

Cessna T303S/N: T30300286

Accident Details

Date
Saturday, August 17, 2019
NTSB Number
ERA19FA249
Location
Lagrangeville, NY
Event ID
20190818X75840
Coordinates
41.700000, -73.729164
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

A partial loss of engine power in both engines during initial climb for reasons that could not be determined based on the available information.

Aircraft Information

Registration
N303TL
Make
CESSNA
Serial Number
T30300286
Engine Type
Reciprocating
Year Built
1984
Model / ICAO
T303C303
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
PEGASUS AVIATION INC
Address
3511 SILVERSIDE RD
Status
Deregistered
City
WILMINGTON
State / Zip Code
DE 19810-4902
Country
United States

Analysis

HISTORY OF FLIGHT

On August 17, 2019, about 1613 eastern daylight time, a Cessna T303, N303TL, was destroyed when it was involved in an accident in Lagrangeville, New York. The private pilot and one person on the ground were fatally injured. Two passengers and one person on the ground sustained serious injuries, and one person on the ground sustained minor injuries. The airplane was operated as a 14 Code of Federal Regulations Part 91 personal flight.

According to the passenger seated in the copilot’s seat, on the morning of the accident the pilot and two passengers departed Republic Airport (FRG) and flew to Orange County Airport (MGJ), Montgomery, New York, where the pilot had a business meeting. After the meeting, they departed MGJ for the return flight to FRG, which included a stop at Sky Acres Airport (44N) in Lagrangeville, New York, to purchase fuel. The passenger reported that the flight from FRG to MGJ and the flight from MGJ to 44N were uneventful. He recalled that the pilot performed an engine runup prior to departing FRG; he did not recall if one was performed prior to the departure from MGJ or prior to the accident flight. The pilot fueled the airplane at 44N, where fuel records indicated he purchased 100 gallons of 100LL aviation fuel.

A review of surveillance video revealed that the airplane engines were shut down for about 10 minutes while the pilot and one of the passengers added fuel to both wing tanks. After the fueling, they did not take any fuel samples from the airplane’s sump drains. After the pilot and both passengers boarded the airplane, the pilot made several unsuccessful attempts to start the left engine for about 30 seconds. Next, the pilot attempted to start the right engine several times over a period of about 30 seconds. During the last attempt, the engine started. The left engine was then started after about 10 seconds of engine cranking. No smoke was visible at any time during the engine start attempts. The airplane remained in position with the engines idling for about 2 minutes before it taxied around to the opposite side of the fuel pump and stopped for about 45 seconds with the engines at or near idle. The pilot then taxied from the fuel pump to runway 17 and did not appear to stop for an engine run-up (although the airplane was out of the camera view for about 14 seconds near the end of the taxiway). The pilot performed a rolling takeoff, and the airplane lifted off the runway in the vicinity of the windsock, which was located on the left side of the runway about 2,100 ft from the runway 17 threshold.

According to the passenger in the copilot’s seat, shortly after liftoff at an altitude of less than 50 to100 ft, both engines lost partial power. They did not stop completely but sounded as though they were “not getting full RPM.” The engines began “stuttering,” which continued until impact with the house. As the airplane proceeded down the runway, it began to drift toward the left until they were over the grass next to the runway. The pilot corrected the drift and the airplane then tracked straight and remained over the grass. As the airplane continued beyond the end of the runway, it was not climbing, and the passenger noticed obstacles that he described as trees and a structure or building. The pilot pitched the airplane up to clear those obstacles. The airplane then began a left turn and as it reached the house the left wing struck the ground, and the right wing struck a tree and the house. The airplane had “very little forward motion” after the initial impact. The passenger estimated that the airplane remained below 100 ft of altitude for the entire flight. He reported that the pilot continued to fly the airplane until impact and did not make any radio calls or say anything to the passengers. He did not hear any warning bells or alarms during the flight. The pilot and both passengers wore their seatbelts and shoulder harnesses.

The airport manager who was mowing the grass at the airport described the airplane’s rotation as “very abrupt” compared to other light twin airplanes he has observed taking off at the airport. Immediately after rotation, he noticed the airplane maintained very shallow bank angles; however, the nose was “high”, and the airplane appeared to yaw slightly to the left. The airplane appeared to correct toward the right before he lost sight of it behind the airport fuel tank. When the airplane emerged from the other side of the tank, the nose was initially lower, but then it pitched up again near the end of the runway before it disappeared behind some trees. The airport manager was wearing ear protection and listening to music and did not hear any engine noise.

Another witness reported that the airplane was “went in a straight line for a short distance and then quickly turned left about 40-45°” which she described as appearing “deliberate and controlled.” She added that she was “surprised the left wing didn’t dip down as the airplane turned. The wings looked like they were steady and pretty parallel to the ground during and after the turn.”

A review of Federal Aviation Administration (FAA) recorded automatic dependent surveillance – broadcast data revealed that after the airplane reached the end of the runway, it climbed from about 675 ft to 775 ft pressure altitude (about 20 to 120 ft above ground level [agl]) in a gradual left turn. During this time the calculated groundspeed decreased from about 80 knots to about 69 knots. The pressure altitude then decreased to 725 ft (about 50 ft agl), the calculated groundspeed decreased to about 66 knots, and the left turn decreased in radius until the recorded data ended about 100 ft west of the accident site.

AIRCRAFT INFORMATION

According to the airplane’s pilot operating handbook (POH), engine mis-starts (without puffs of black smoke) can result from an excessively lean mixture in cold or warm temperatures or by vapor lock in extremely high temperatures. If vapor lock is suspected, the primer switch (which operates the auxiliary fuel pumps) should be turned on for 5 to 10 seconds prior to starting the engine, to flush the vapor through the fuel lines. Additionally, the auxiliary fuel pumps are to be turned on for takeoff, landing, or any time vapor is suspected in the fuel system, such as in hot day/high altitude conditions or conditions during a climb that are conducive to fuel vapor formation.

The POH also prescribes a “Hot Day Takeoff” procedure which includes a static runup of the engines and evaluation of the maximum engine RPM achieved before takeoff. The procedure includes an adjustment to lean the mixture, if necessary, to ensure sufficient engine RPM and establish a required minimum fuel flow, prior to takeoff. The normal maximum RPM achieved during the procedure should be 2,400 and must be at least 2,300. The procedure does not specify an ambient temperature range for which the procedure is required but does specify that it should be performed “on warm humid or hot days with heated engine(s) and oil and cylinder temperatures near mid-scale or higher.” It prescribes adjustments and performance calculation penalties if the maximum RPM achieved is between 2,300 and 2,400.

METEOROLOGICAL INFORMATION

At 1653, the weather conditions at Hudson Valley Regional Airport (POU), Poughkeepsie, New York, located about 8 miles southwest of the accident site included temperature 30° C, dewpoint 20° C, wind from 170° at 7 knots, and an altimeter setting 29.93 inches of mercury. The density altitude calculated for the takeoff at 44N (field elevation 697 ft) was 2,633 ft.

WRECKAGE AND IMPACT INFORMATION

Examination of the wreckage revealed that most of the fuselage forward of the aft bulkhead was destroyed by fire. Except for the empennage, most of the wreckage that remained was found within the right (north) half of the house foundation perimeter. The north half of the house structure and roof was consumed by fire. The empennage remained largely intact and was found with the right horizontal stabilizer leaning against what remained of the rear wall of the house, oriented on a heading of about 030° magnetic. The damaged left wingtip, left engine, right engine, and the right (green) navigation light lens were found oriented along a line from the rear of the house to a bush by the front wall of the house, roughly the length of the wingspan and oriented perpendicular to the empennage. The cabin heater, which was mounted in the nose of the airplane, was found about 15 ft away from and in line with the orientation of the empennage.

Flight control continuity was confirmed from what remained of the flight control tubes near the cockpit, to the rudder, the elevator and to the outboard aileron bell cranks in each wing. Neither of the aileron pushrods were found. All cable ends were found at their respective attachment points. The right aileron cable was fractured in one location near the bell crank. The rudder and elevator trim actuators were near the neutral position. The aileron trim condition could not be determined. The remnants of the landing gear were found in the retracted position. The flap jackscrew actuator was consistent with the retracted position. All of the cockpit instruments were consumed by fire, and none were located except for one 2-inch diameter dial face that was illegible but consistent with a vacuum gauge. A metal avionics rack was located with ash inside. Several loose metal unidentified toggle switches were found near the cockpit area. Neither of the two electric fuel boost pumps were located. Remnants of both fuel selector valves were found; however, both were too thermally damaged to determine their position.

The cockpit engine and propeller controls were located; however, the preimpact position of the levers and the cable continuity to each engine could not be determined due to thermal damage.

Several spark plugs, rocker arm assemblies, and pushrods were found loose in...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA19FA249