N501SF

Substantial
None

Cessna T210S/N: 21061808

Accident Details

Date
Tuesday, August 20, 2019
NTSB Number
WPR19LA237
Location
Eugene, OR
Event ID
20190820X13813
Coordinates
44.123611, -123.202220
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The failure of the landing gear electric motor to shut off after landing gear retraction, which resulted in the motor overheating, burning out, and producing smoke in the cockpit. The pilot’s decision to land with the landing gear retracted resulted in substantial damage to the airplane.

Aircraft Information

Registration
Make
CESSNA
Serial Number
21061808
Engine Type
Reciprocating
Model / ICAO
T210T210
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
T210M

Registered Owner (Current)

Name
NOMARCO INC
Address
4066 S ELLIOTT PRAIRIE RD
City
WOODBURN
State / Zip Code
OR 97071-8755
Country
United States

Analysis

On August 20, 2019, about 1435 Pacific daylight time, a Cessna 210M airplane, N501SF, was substantially damaged when it was involved in an accident near Eugene, Oregon. The student pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 instructional flight.

The student pilot reported that the accident flight was his third supervised solo flight. Shortly after departure, at an altitude of about 3,000 ft mean sea level, he smelled smoke in the cockpit. He returned to the departure airport, where he performed a gear-up landing, resulting in substantial damage to the airplane. The pilot mentioned that he elected not to attempt to lower the landing gear with the landing gear selector switch, nor to utilize the emergency landing gear extension procedure. The pilot stated, “I thought I was on fire and just wanted to get the airplane on the ground.”

An examination by a mechanic revealed that the electric motor that powered the hydraulic power pack pump for the landing gear was still powered after the accident. The mechanic stated that he believed the motor did not shut off during the gear retraction and that this would have caused it to overheat and burn out, resulting in smoke in the cockpit. He was not able to determine why the motor failed to shut off as designed. The pilot did not report any additional mechanical anomalies with the airplane or engine that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19LA237