N714LK

Destroyed
Fatal

Cessna 150S/N: 15079256

Accident Details

Date
Monday, November 4, 2019
NTSB Number
ERA20FA031
Location
New Bedford, MA
Event ID
20191104X71357
Coordinates
41.621112, -70.938331
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Pilot impairment due to exposure to carbon monoxide as a result of undetected corrosion and holes in the engine’s left exhaust muffler.

Aircraft Information

Registration
N714LK
Make
CESSNA
Serial Number
15079256
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
150C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
VIDAL PAUL E
Address
5 FIGERADO ST
Status
Deregistered
City
WESTPORT
State / Zip Code
MA 02790-3107
Country
United States

Analysis

HISTORY OF FLIGHTOn November 4, 2019, at 1532 eastern standard time, a Cessna 150M, N714LK, was destroyed when it was involved in an accident near New Bedford, Massachusetts. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to an employee of the fixed based operator at the New Bedford Regional Airport (EWB), New Bedford, Massachusetts, where the owner/pilot based his airplane, the pilot was “cheerful and happy to be flying” the morning of the accident. He reported that the pilot spent about 10 to 15 minutes performing a preflight inspection of his airplane before departing.

Automatic dependent surveillance-broadcast (ADS-B) data obtained from the Federal Aviation Administration (FAA) indicated that the airplane departed EWB around 1450 and climbed to about 2,500 ft mean sea level (msl) while tracking in a southwesterly direction for about 20 minutes. The airplane then began a gradual descent, turned to the northeast, and flew along the shoreline. It then proceeded to fly north toward EWB, descending to around 250 ft above ground level over a golf course fairway less than 3 nm from EWB. The airplane then commenced a climbing right turn at increasing pitch attitudes to an altitude of about 4,000 ft msl, when the airplane then descended rapidly in a left circular pattern.

According to a witness who had exited his car in a parking lot near the accident site, he heard a sound "like a motor revving up high." He looked up and saw an airplane "swoop down like it was going to land,” climb very high, and then “pivot on its left wing” before “coming straight down.” He thought the airplane was “doing tricks.”

Examination of the accident site and wreckage revealed that the airplane impacted a tree in a cemetery in a near vertical nose-down attitude.

PERSONNEL INFORMATIONInterviews with friends and acquaintances of the pilot revealed that it was highly unusual and uncharacteristic behavior for the pilot to perform aerobatics. They considered him to be a very conservative pilot.

According to a friend of the pilot who flew with him regularly, the pilot often flew toward Newport, Rhode Island, and then along the shoreline back toward West Island, Massachusetts, where the pilot would typically contact the EWB air traffic control tower when inbound for landing.

According to the president of the EWB fixed based operator, the business staff monitored the tower frequency for incoming airplanes and did not hear the pilot make any radio transmissions, adding that the pilot “would never enter the airspace without calling.”

AIRCRAFT INFORMATIONCabin Heat System

According to the Cessna 150 Pilot Operating Handbook, “the temperature and volume of airflow into the cabin can be regulated to any degree by manipulation of the push-pull CABIN HT and CABIN AIR control knobs.” The left engine muffler was constructed with a shroud around the outside, which forms a heating chamber for the cabin heater air. The heated air from the muffler shroud is then routed to the cabin when the CABIN HT knob is pulled out.

Maintenance and Muffler History

A logbook entry indicated that the muffler was last replaced June 1, 2004, at tachometer time 4,321.5 hours, or 742.9 hours before the accident flight; however, the maintenance entry did not specify which muffler was replaced.

The mechanic who performed the most recent annual inspection stated that he opened each muffler shroud to inspect the muffler, looking for stains, soot or cracks, which would indicate the need to change the muffler. He stated that he found no anomalies during the muffler inspections.

The airplane was not equipped with any type of carbon monoxide (CO) detector.

The inspection chart contained in the Model 150 Series (1977) Service Manual indicates that a general inspection of the exhaust system should be conducted every 50 hours and references a more detailed procedure later in the manual for an inspection every 100 hours. The 100-hour inspection information starts by stating, “Inspection of the exhaust system shall be thorough because the cabin heating system uses air heated by the heat exchangers of the exhaust system. Since exhaust systems of this type are subject to burning, cracking, and general deterioration from alternate thermal stresses and vibration, inspection is very important and should be accomplished every 100 hours of operation. The airplane was generally inspected on an annual basis, and not a 100-flight hour basis. A review of the maintenance records indicated that the annual inspections occurred at flight hour intervals ranging from 39 hours to 55 hours in the 10 years preceding the accident flight.

AIRPORT INFORMATIONCabin Heat System

According to the Cessna 150 Pilot Operating Handbook, “the temperature and volume of airflow into the cabin can be regulated to any degree by manipulation of the push-pull CABIN HT and CABIN AIR control knobs.” The left engine muffler was constructed with a shroud around the outside, which forms a heating chamber for the cabin heater air. The heated air from the muffler shroud is then routed to the cabin when the CABIN HT knob is pulled out.

Maintenance and Muffler History

A logbook entry indicated that the muffler was last replaced June 1, 2004, at tachometer time 4,321.5 hours, or 742.9 hours before the accident flight; however, the maintenance entry did not specify which muffler was replaced.

The mechanic who performed the most recent annual inspection stated that he opened each muffler shroud to inspect the muffler, looking for stains, soot or cracks, which would indicate the need to change the muffler. He stated that he found no anomalies during the muffler inspections.

The airplane was not equipped with any type of carbon monoxide (CO) detector.

The inspection chart contained in the Model 150 Series (1977) Service Manual indicates that a general inspection of the exhaust system should be conducted every 50 hours and references a more detailed procedure later in the manual for an inspection every 100 hours. The 100-hour inspection information starts by stating, “Inspection of the exhaust system shall be thorough because the cabin heating system uses air heated by the heat exchangers of the exhaust system. Since exhaust systems of this type are subject to burning, cracking, and general deterioration from alternate thermal stresses and vibration, inspection is very important and should be accomplished every 100 hours of operation. The airplane was generally inspected on an annual basis, and not a 100-flight hour basis. A review of the maintenance records indicated that the annual inspections occurred at flight hour intervals ranging from 39 hours to 55 hours in the 10 years preceding the accident flight.

WRECKAGE AND IMPACT INFORMATIONExamination of the accident site and wreckage revealed that the airplane impacted a tree in a near vertical nose down attitude about 3.5 nautical miles and about 164° magnetic from EWB. The debris field extended about 240 ft from the tree on a heading of about 220°. The left wing with the strut attached was located about 10 ft from the tree, followed by the empennage, cabin and engine at 30 ft, the right wing at 40 ft, the carburetor at 87 ft, a ruptured fuel tank at 122 ft, and the main wheels and directional gyro at 240 ft. All major components of the airplane were present at the accident site.

The fuselage was significantly fragmented. Both wings were impact fractured, bent on all surfaces, and exhibited leading edge damage consistent with tree impact. The empennage was impact fractured and bent. The instrument panel was largely fragmented. The engine controls were in the full forward position. The cabin heat control was in the full aft (ON) position.

The engine was examined, and no pre-impact anomalies were noted that would have prevented normal production of power.

The propeller remained attached to the engine crankshaft propeller flange. Examination of the propeller blades revealed aft bending and twisting along the length of both blades with leading-edge gouging and chordwise rotational scoring on the camber sides. Control continuity was established from the flight controls through overload fractures to the control surfaces.

The left muffler outer casing was impact crushed exposing the end plate which exhibited an erosion hole and several other smaller pin holes. The cabin heat shroud was removed from the muffler, and additional evidence of internal deterioration was present. The muffler metal was corroded and thin, and pin holes were observed on the sides of the muffler. The right muffler was crushed and compacted, and the shroud, which provides heated air to the carburetor heat control, remained intact around the muffler.

ADDITIONAL INFORMATIONFAA Carbon Monoxide and Exhaust System Guidance

On November 24, 1972, the FAA issued advisory circular (AC) 20-32B "Carbon Monoxide (CO) Contamination in Aircraft—Detection and Prevention." The AC provided information on the potential dangers of carbon monoxide contamination from faulty engine exhaust systems or cabin heat exchangers. It also discussed means of detection and procedures to follow when contamination is suspected.

In October 2009, the FAA issued report DOT/FAA/AR-09/49, "Detection and Prevention of Carbon Monoxide Exposure in General Aviation Aircraft." The report documented research on detection and prevention of CO exposure in general aviation aircraft, with the objective of identifying exhaust system design issues related to CO exposure, evaluating inspection methods and maintenance practices with respect to CO generation, and the identification of protocols to quickly alert users to the presence of excessive CO in the cockpit and cabin.

On March 17, 2010, the FAA published Special Airworthiness Information Bulletin (SAIB) CE-10-19 R1. It recommended that owners and operators of general aviation aircraft consider the infor...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA20FA031