N50JR

Substantial
Minor

Beech 60S/N: P-303

Accident Details

Date
Wednesday, January 29, 2020
NTSB Number
CEN20TA071
Location
Big Spring, TX
Event ID
20200129X95515
Coordinates
32.059722, -101.585830
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power in both engines due to fuel exhaustion, which resulted in a landing short of the runway.

Aircraft Information

Registration
N50JR
Make
BEECH
Serial Number
P-303
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
7X OILFIELD SERVICES INC
Address
1009 S JACKSON ST
Status
Deregistered
City
MIDLAND
State / Zip Code
TX 79701-8378
Country
United States

Analysis

On January 29, 2020, about 1710 central standard time, a Beechcraft BE60 airplane, N50JR, sustained substantial damage when it was involved in an accident about ½ mile southwest of Edwards Lucian Wells Ranch Airport (TX31), Big Spring, Texas. The commercial pilot and sole occupant received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, before departing Abilene Regional Airport (KABI), Abilene, Texas for Odessa Airport (KODO), Odessa, Texas, he asked the fixed base operator (FBO) to add 20 gallons of 100LL aviation gasoline to both fuel tanks. Fuel receipts and statements from FBO personnel confirm that the fuel requested was added to the airplane.

A review of Federal Aviation Administration (FAA) archived air traffic control (ATC) communications revealed that after departing KABI, the pilot climbed to a cruising altitude of 10,500 ft. At 1656, the pilot advised ATC of left engine issues and indicated they may have to land at Big Spring, Texas (KBPG). At 1659, the pilot confirmed that he intended to land at KBPG. At 1700, the pilot informed ATC that the right engine was running and the left engine was shut down. He stated that he was able to maintain altitude and wished to continue to KODO. About one minute later, the pilot, once again, advised ATC that he would continue to KODO and would not need assistance upon arrival. Shortly thereafter, the pilot requested a heading for KBPG and stated that the right engine had failed.

At 1703, ATC asked the pilot if he would make it to the airport, to which he replied that he may not, but was trying. After being offered an alternate airport by ATC, the pilot stated that he preferred KBPG and reported the airport in sight. At 1704, the pilot called ATC and told them the engine was failing and he saw a different airport that he would attempt a landing at. About 1705, the pilot notified ATC that he was over the airport and would try to land. About a minute later, the pilot stated that he was entering the traffic pattern for the runway and was going to be able to make it. About 1707, the pilot stated that he was on left downwind for the airport and was 90% sure he could make the airport. About two minutes later, another airplane on the same frequency told ATC that he was hearing the broadcast of an emergency locator transmitter and heard a transmission, "I'm going to crash."

The wreckage was located about 10 minutes later 200 to 300 yards before the threshold of runway 02. The airplane came to rest upright and sustained substantial damage to the wings and fuselage.

The pilot later reported to the NTSB that about 10 miles east of KBPG, both engines lost power due to a "lack of fuel flow." Following the loss of engine power, he looked for a place to land and saw TX31 that appeared to be within gliding distance. He overflew the airport and turned onto final for the north runway. On short final, he lowered the landing gear and "the plane quit flying, the airspeed went to nothing and the plane landed short of the runway."

When the FAA aviation safety inspector arrived on scene, they attempted to drain fuel from the fuel tanks. They were able to drain "a couple tablespoons" of fuel from the left tank, but were unable to drain the right tank due to the terrain and the position of the airplane. There was no blue discoloration present on either of the wings or engine nacelles and neither fuel tank was breached. The battery remained connected, and when power was applied to the electrical system, both fuel quantity gauges indicated empty.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20TA071