N280MM

Destroyed
Fatal

Enstrom 280S/N: 2099

Accident Details

Date
Wednesday, June 24, 2020
NTSB Number
WPR20LA191
Location
Hayden, ID
Event ID
20200623X23649
Coordinates
47.775001, -116.895550
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The total loss of power while maneuvering at low altitude due to the detonation of two engine cylinders and damaged spark plugs. 

Aircraft Information

Registration
N280MM
Make
ENSTROM
Serial Number
2099
Engine Type
Reciprocating
Year Built
2003
Model / ICAO
280EN28
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
CHARBONNEAU J R
Address
12404 E SHAWNEE DR
Status
Deregistered
City
SPOKANE
State / Zip Code
WA 99206-9302
Country
United States

Analysis

HISTORY OF FLIGHTOn June 23, 2020, about 1701 Pacific daylight time, an Enstrom 280 FX helicopter, N280MM, was destroyed when it was involved in an accident near Hayden, Idaho. The student pilot was fatally injured, and the flight instructor was seriously injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

The flight instructor stated that, shortly after takeoff from Coeur d’Alene Airport, Coeur d’Alene, Idaho, he temporarily leveled off the helicopter at an altitude of about 100 ft above ground level and accelerated to more than 100 mph to ensure that all the helicopter systems and indications were properly functioning. Shortly thereafter, the engine’s rpm “skyrocketed,” and the engine lost total power; the flight instructor could hear “backfiring.” The helicopter then lost altitude, and the flight instructor maneuvered the helicopter to avoid nearby power lines. Subsequently, the low rotor rpm horn sounded; at that time, the engine was still running. As terrain approached, the flight instructor pulled the collective and increased the throttle, but the helicopter had no rpm. Shortly afterward, the helicopter impacted terrain, the main rotor blades contacted the tailboom, and the helicopter spun about 180° before coming to rest. A postcrash fire ensued, which consumed most of the helicopter.

According to witnesses, the helicopter was maneuvering at a low altitude before it crashed in an open field. Two witnesses stated that the helicopter was flying at or below the power line level. One witness stated that the tail of the helicopter was moving up and down and that the helicopter did not seem to be flying smoothly. The witness further stated that the helicopter’s tail swung around quickly before ground impact. One witness who provided assistance after the accident reported the student pilot stating that the helicopter was losing power and that the helicopter did not strike anything before ground impact.

AIRCRAFT INFORMATIONThe engine maintenance logbook revealed that the engine time since overhaul was 407.4 hours. The logbook showed that, during the annual inspection on July 15, 2019 (almost 1 year before the accident), the mechanic performing the inspection “cleaned [the spark] plugs.”

The Enstrom height and velocity diagram revealed that the helicopter’s altitude and airspeed before the accident were not within the shaded regions, which represented areas, altitudes, and airspeeds to avoid during operation.

AIRPORT INFORMATIONThe engine maintenance logbook revealed that the engine time since overhaul was 407.4 hours. The logbook showed that, during the annual inspection on July 15, 2019 (almost 1 year before the accident), the mechanic performing the inspection “cleaned [the spark] plugs.”

The Enstrom height and velocity diagram revealed that the helicopter’s altitude and airspeed before the accident were not within the shaded regions, which represented areas, altitudes, and airspeeds to avoid during operation.

WRECKAGE AND IMPACT INFORMATIONThe Kootenai County Sheriff’s Office responded to the accident site, which was in a field northwest of a road intersection. The Kootenai County Fire Department extinguished the postaccident fire. The wreckage was surrounded by a burnt area on the ground that was about 45 ft in diameter. The front section of the fuselage came to rest on a northeast heading. The tail rotor assembly was located west of the wreckage.

A postaccident examination of the helicopter revealed extensive thermal damage, which prevented a thorough examination of most systems and components. The tailboom was separated from the fuselage, and the horizontal stabilizer was separated from the tailboom. The engine also sustained thermal damage.

An engine examination revealed no evidence of a catastrophic mechanical malfunction or failure and no anomalies with the transmission. When the top and bottom spark plugs were removed, the examination showed that the No. 3 cylinder bottom spark plug was missing part of its center electrode, and that the No. 4 cylinder bottom spark plug was missing its electrode. Furthermore, when all six cylinders were removed, the No. 2 cylinder piston was found to exhibit a sandblasted appearance consistent with detonation. Additionally, the No. 4 cylinder head and piston exhibited signatures and damage consistent with detonation.

ADDITIONAL INFORMATIONThe Federal Aviation Administration’s Airplane Flying Handbook states the following about detonation:

Detonation, as the name suggests, is an explosion of the fuel-air mixture inside the cylinder. During detonation, the fuel/air charge (or pockets within the charge) explodes rather than burns smoothly. Because of this explosion, the charge exerts a much higher force on the piston and cylinder, leading to increased noise, vibration, and cylinder head temperatures. The violence of detonation also causes a reduction in power. Mild detonation may increase engine wear, though some engines can operate with mild detonation regularly. However, severe detonation can cause engine failure in minutes.

The handbook also stated, “excessive cylinder temperature can lead to detonation, which in turn can cause catastrophic engine failure.”

Additionally, the Federal Aviation Administration Aviation Maintenance Technician Handbook—General stated that “detonation causes explosive burning of the fuel which creates an increased cylinder pressure, excessive cylinder head temperatures, and decreased engine performance.” According to the engine manufacturer, “severe or prolonged detonation can cause damage to the cylinder head and pistons. In some extreme cases, the connecting rod can be bent or broken, the cylinder head may crack or fail, or the piston ring lands may break.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20LA191