N777CP

Substantial
None

BELL 206S/N: 3429

Accident Details

Date
Friday, October 16, 2020
NTSB Number
ERA21LA023
Location
Zephyrhills, FL
Event ID
20201019102161
Coordinates
28.338616, -81.957469
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Improper torquing of the “B” nut at the fuel control unit, which led to a total loss of engine power and subsequent autorotation that resulted in substantial damage.

Aircraft Information

Registration
Make
BELL
Serial Number
3429
Engine Type
Turbo-shaft
Model / ICAO
206B06
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
5
FAA Model
206B

Registered Owner (Current)

Name
WILD GOOSE AIRWAYS OF PLANT CITY LLC
Address
11715 TAYLOR RD
City
THONOTOSASSA
State / Zip Code
FL 33592-3027
Country
United States

Analysis

On October 16, 2020, about 1515 eastern daylight time, a Bell 206B, N777CP, was substantially damaged when it was involved in an accident near Zephyrhills, Florida. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, about 15 minutes after departure, he heard a “binding sound” and felt a reduction in engine power and a slight nose left yaw. He checked his engine instruments and noted no illumination of annunciator lights or engine warnings. The low rotor rpm aural alarm then sounded, and he initiated an autorotation to swampy terrain.

According to the Federal Aviation Administration inspector who responded to the accident site, the helicopter came to rest among pine trees and undergrowth. The tailboom was impactseparated, and the main rotors were fractured about midspan.

A detailed examination revealed the “B” nut at the engine fuel control unit was loose with no thread engagement. The nut was also missing the torque stripe markings on the line as required by the Rolls-Royce maintenance manual. During a test run of the engine, the “B” nut was tightened and torqued to proper specification. The engine ran smoothly and continuously at all power settings.

A review of the helicopter’s maintenance records revealed the last annual inspection was completed about 75 hours prior to the accident. At that time, the Nos. 1 and 2 turbine wheels were replaced. The pilot also holds an airframe and powerplant certificate and was the last person to perform maintenance on the engine.

According to the Rolls-Royce maintenance manual, torque paint must be applied to all the rigid tube “B” nuts and reapplied each time the nut is loosened and tightened. The manual states that “Proper tightening of the engine tubing connections is critical to flight safety. Failure to properly install, align, and tighten fuel, oil, and air fittings cold result in an engine failure.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA21LA023