N383DB

Substantial
Fatal

VANS RV7S/N: 72319

Accident Details

Date
Monday, February 22, 2021
NTSB Number
ERA21FA135
Location
Mayfield, KY
Event ID
20210223102659
Coordinates
36.779157, -88.584105
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall, loss of airplane control, and subsequent impact with terrain.

Aircraft Information

Registration
N383DB
Make
VANS
Serial Number
72319
Engine Type
Reciprocating
Year Built
2011
Model / ICAO
RV7RV7
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BABENCO HENRY D
Address
6350 CLINTON RD
Status
Deregistered
City
PADUCAH
State / Zip Code
KY 42001-9394
Country
United States

Analysis

On February 22, 2021, about 1756 central standard time, an experimental, amateur-built Vans RV-7A airplane, N383DB, was substantially damaged when it was involved in an accident near Mayfield Graves County Airport (M25), Mayfield, Kentucky. The private pilot was fatally injured. The airplane was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.

A witness at M25 stated the airplane was conducting touch-and-go landings on runway 1. Another witness traveling eastbound on a nearby interstate saw the airplane climbing and reported that, “as the airplane went higher…the tail dropped, and the plane went into a back flip. This witness then observed the airplane come out of the “flip” and descend “nose first” toward the ground. The airplane subsequently impacted an open field located about 1,011 ft north of the airport. Another witness reported that he observed the airplane takeoff and noted that it was climbing at a high angle of attack.

The wreckage was confined to a small area. All airplane components were accounted for at the accident site, and flight control continuity was confirmed for all control surfaces. The wings exhibited symmetrical accordion-type crushing damage and remained attached to the fuselage. Both wing fuel tanks were breached, and both fuel main caps were found in place. The empennage, main landing gear, and all control surfaces also remained attached to the fuselage. The engine and nose landing gear separated from the forward fuselage.

The engine was rotated by hand at the accessory gear section, and crankshaft continuity was confirmed. Thumb compression was attained on all cylinders. The engine-driven fuel pump contained 100 low-lead aviation fuel and produced suction and pressure when activated by hand. The left magneto was impact damaged and was not able to be rotated. The right magneto produced spark on all towers. The two-bladed propeller was found fractured from the engine due to impact forces. One blade exhibited rearward bending and leading-edge gouges, and the other blade exhibited Sbending.

Examination of the airframe and engine revealed no preimpact mechanical malfunctions or anomalies that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA21FA135