N9199S

Substantial
Serious

BEECH B24RS/N: MC-371

Accident Details

Date
Thursday, May 13, 2021
NTSB Number
CEN21LA219
Location
New Lenox, IL
Event ID
20210513103082
Coordinates
41.552400, -87.980600
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
3
Minor Injuries
1
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The total loss of engine power due to fuel contamination as a result of the pilot’s improper fueling of the airplane.

Aircraft Information

Registration
N9199S
Make
BEECH
Serial Number
MC-371
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
B24RBE24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BENEDETTI NICHOLAS
Address
347 W CHESTNUT ST UNIT 2211
Status
Deregistered
City
CHICAGO
State / Zip Code
IL 60610-3025
Country
United States

Analysis

On May 13, 2021, at 1117 central daylight time, a Beech B24R airplane, N9199S, was substantially damaged when it was involved in an accident near New Lenox, Illinois. The pilot and 2 passengers were seriously injured, and 1 passenger sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported the airplane was fueled from four identical fuel containers kept in the flying club hangar. One container was already full. He took the other three containers to the fuel pump, filled them with 100 low-lead aviation fuel, and returned to the airplane. He added about 10 gallons of fuel to each wing fuel tank from the four containers. Shortly afterward, during the preflight inspection, he sumped the fuel tanks and did not observe any contamination. The engine started without hesitation, and the before takeoff run-up, takeoff, and initial climb out were normal. The right fuel tank was selected for the takeoff and initial climb; however, he then switched the left fuel tank. Shortly after changing tanks, the engine lost power. His efforts to restore engine power were not successful, and he executed a forced landing to an interstate highway. The airplane impacted a concrete barrier wall during the landing.

A postaccident examination recovered approximately 2-1/2 gallons of water from the left fuel tank. No water was detected in the right fuel tank. No anomalies with respect to the engine assembly or the airframe fuel system were observed.

An individual associated with the flying club reported that he was cleaning an airplane in the hangar the day before the accident flight. He had used a fuel container to get water and marked it, “water for cleaning”. At the end of the day, he left the container next to the airplane with the intention of continuing the next day. There were 2 to 3 gallons of water in the container at the time.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN21LA219