Accident Details
Probable Cause and Findings
The pilot was unable to stop the airplane during the landing for reasons which could not be determined, resulting in a runway excursion.
Aircraft Information
Registered Owner (Historical)
Analysis
On September 3, 2021, about 1244 eastern daylight time, a Raytheon Aircraft Company 390, N351CW, was substantially damaged when it was involved in an accident at Naples Municipal Airport (APF), Naples, Florida. The pilot and three passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 135 on-demand flight.
According to the pilot, the takeoff and en route portions of the flight were uneventful. During landing, he applied normal braking and the airplane started to slow down. Suddenly the brakes “faded away,” and he was unable to stop the airplane. He further described that he applied full braking pressure and the pedals were operating as they should, but the airplane was not stopping. He added that every few feet the brakes would grab, lock-up for a few feet, and then release. The brakes grabbed several times during the landing roll but were not slowing the airplane down. The airplane overran the end of the runway, and the pilot steered the airplane into the grass and away from a jet blast fence.
A Federal Aviation Administration inspector who examined the airplane after the accident observed that the airplane sustained substantial damage to both wings during the runway excursion.
The pilot reported the runway surface condition as “damp.” He further stated that it was not raining, there was no standing water on the runway and “If I had to choose between the descriptor of either wet or dry as my only options, I would choose dry.”
According to automatic dependent surveillance broadcast (ADS-B) data, the airplane made a normal Vref approach and landed about 8 knots higher than the landing chart for 10,200 lbs about 110 knots. The runway length was 6,600 ft and about 4,500 ft of runway remained for the airplane to stop. The landing chart in the airplane flight manual (AFM) revealed that about 3,000 ft was required for landing on a dry runway, and about 3,750 ft was required for a wet runway.
The anti-skid box, brake valve, anti-skid valve, and both wheel speed transducers were removed and sent to the manufacturer for testing. All the components passed the tests, and no anomalies were noted.
The airplane was not equipped with a flight data recorder. The cockpit voice recorder was removed and sent the National Transportation Safety Board’s recorders laboratory for download.
The airplane was not equipped with thrust reversers. The wind was reported from 150° at 5 knots, at APF, at 1235.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA21LA350