N677JD

Substantial
Serious

STINSON 108S/N: 108-416

Accident Details

Date
Friday, October 8, 2021
NTSB Number
CEN22LA012
Location
Wildwood, AR
Event ID
20211012104081
Coordinates
35.017152, -92.070303
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined.

Aircraft Information

Registration
N677JD
Make
STINSON
Serial Number
108-416
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
108S108
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
257 OLD CHURCHMANS RD
Status
Deregistered
City
NEW CASTLE
State / Zip Code
DE 19720-1529
Country
United States

Analysis

On October 8, 2021, about 1325 central daylight time, a Stinson 108 airplane, N677JD, sustained substantial damage when it was involved in an accident near Wildwood, Arkansas. The pilot sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal cross-country flight.

The pilot reported that after he leveled from a descent and increased throttle, the engine “began to cough and cut out intermittently.” Shortly thereafter, the engine lost all power, and the propeller began to windmill. He immediately verified the mixture was full rich, applied the carburetor heat, and checked the magnetos, but could not restore engine power. He stated that about 10 minutes before the loss of engine power, he had switched from the right fuel tank to the left fuel tank, which had about 13 gallons of fuel remaining. The pilot executed a forced, power-off landing to a golf course, and the airplane impacted a tree, which resulted in substantial damage to the fuselage and left wing.

During a postaccident examination of the Franklin 6A4-150-B3 engine, fuel was ejected from the carburetor when the butterfly valve was manipulated. The top spark plug from the No. 2 cylinder was bright white, consistent with exposure to high heat, and the No. 5 cylinder and piston contained evidence of oil present past the cylinder rings. Both magnetos were removed and tested using a hand drill with all terminals producing bright blue spark. No obstructions were noted within the air induction system and the examination revealed no pre-impact mechanical malfunctions or anomalies that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA012