N8AU

Substantial
Fatal

BELL 206BS/N: 4089

Accident Details

Date
Thursday, December 30, 2021
NTSB Number
CEN22FA086
Location
Livingston, TX
Event ID
20211230104459
Coordinates
30.648176, -94.915110
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot exceeding the yaw control capability of the helicopter for the flight conditions, resulting in a non-mechanical loss of tail rotor effectiveness.

Aircraft Information

Registration
Make
BELL
Serial Number
4089
Engine Type
Turbo-shaft
Year Built
1990
Model / ICAO
206BB06
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
5
FAA Model
206B

Registered Owner (Current)

Name
DODSON INTERNATIONAL PARTS INC
Address
2155 VERMONT RD
City
RANTOUL
State / Zip Code
KS 66079-9014
Country
United States

Analysis

HISTORY OF FLIGHTOn December 30, 2021, about 1141 central standard time, a Bell 206B helicopter, N8AU, was substantially damaged during an accident near Livingston, Texas. The pilot and one passenger were fatally injured, and two passengers received minor injuries. The flight was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.

Automatic dependent surveillance - broadcast data for the flight showed that the helicopter departed the Livingston Municipal Airport (00R) about 1107 and headed east-northeast for about 25 nautical miles (nm) before reversing course to a west-southwest direction. The helicopter then turned further south before the end of the data at 1138. The final recorded location was 1.8 nm northeast of the accident site.

Figure 1. ADS-B Flight Path Depiction

Video from the front left passenger’s cellular phone showed that the helicopter flew along the road where the passenger’s house was located. The video showed that the helicopter was traveling about 40 kts about 150 ft above ground level before slowing and making a right turn around the house. The helicopter completed about 270° of turn and slowed to a hover before the video ended. The audio portion of the video captured the sounds of the rotors and the engine. No discernable unusual noises were evident in the audio recording. The video and audio ended before the accident occurred.

According to the surviving passengers, the flight was a sightseeing flight that the deceased front-seat passenger had won at a local charity auction. On the day of the accident, the passengers met the pilot at 00R. The original intent was to fly over the deceased passenger’s childhood home near Woodville, TX. While on course toward Woodville, it became evident that the flight could not be continued due to low clouds and the helicopter was then maneuvered to the passenger’s current residence near Livingston, TX. The rear-seat passengers stated that the helicopter flew down the road where the residence was located and then around the house making a level right turn at low speed. The helicopter then flew over a pond on the property and toward the house. As the helicopter approached the house it was facing a south direction and came to a hover above the trees where the accident occurred. The passengers stated that the helicopter was either motionless in the hover or slightly drifting.

Figure 2. Depiction of the Flight Final Path to the Accident Site

Once in the hover, the helicopter began to rotate to the right, which one passenger initially thought was the pilot intentionally maneuvering the helicopter. The helicopter continued to rotate, and the passenger realized the rotation was not intentional. The helicopter rotated about two full revolutions before striking a tree with the rotor blades and descending to the ground. It came to rest on its left side on top of a wood pile that had been created due to land clearing. One passenger noticed, after attending to the pilot and front-seat passenger, that the helicopter’s engine was still running. He started moving any switch he could find to the “off” position until the helicopter’s engine stopped. PERSONNEL INFORMATIONThe pilot held an airline transport pilot certificate with multi-engine land airplane and rotorcraft-helicopter certificates. He also had private pilot privileges for single-engine land airplanes. He reported civil flight experience that included 1679 total and 72 hours in last six months as of his most recent medical exam dated July 15, 2016. He was issued a Second-Class Medical Certificate without limitation on that date. The medical certificate expired for all classes in 2018, but he had applied for BasicMed. The pilot had most recently completed the BasicMed Course on June 7, 2020, and the most recent submission of the required Comprehensive Medical Examination Checklist (CMEC) was on June 13, 2018.

Review of pilot flight records indicated that he had about 200.9 hours of flight experience in helicopters, which included about 71.7 hours in the accident make and model. AIRCRAFT INFORMATIONThe helicopter maintenance records were not available during the investigation; however, the maintenance facility that completed the most recent maintenance provided a copy of the inspections performed. The records provided indicated that the helicopter had received 12-month and 24-month inspections per the manufacturer’s maintenance manual on May 20, 2021. METEOROLOGICAL INFORMATIONUnofficial weather stations located between 5 and 12 miles from the accident site recorded winds from 357° to 196° with magnitudes varying from 1 to 4 kts. The quality of the data from the unofficial sites could not be determined. AIRPORT INFORMATIONThe helicopter maintenance records were not available during the investigation; however, the maintenance facility that completed the most recent maintenance provided a copy of the inspections performed. The records provided indicated that the helicopter had received 12-month and 24-month inspections per the manufacturer’s maintenance manual on May 20, 2021. WRECKAGE AND IMPACT INFORMATIONFigure 3. Helicopter as viewed during on-scene examination (NTSB Photo)

The helicopter impacted terrain and rolled over onto its left side coming to rest on a pile of logs. The forward fuselage and left side fuselage and tail boom sustained substantial damage. The main and tail rotors were separated. The elevation at the accident site was about 250 ft above mean sea level.

Postaccident examination of the helicopter did not reveal any preimpact failures or malfunctions with the airframe, rotor systems, engine, or flight controls that would have precluded normal operations. INJURIES TO PERSONSThe passenger seated in the front left seat of the helicopter was fatally injured in the accident. The pilot, seated in the front right seat, initially survived and was transported to a hospital but succumbed to his injuries 13 days after the accident. The death certificate listed complications following multiple blunt force injuries as the cause of death. FLIGHT RECORDERSThe helicopter was not equipped with on-board flight or data recording equipment; however, the front-seat passenger recorded the flight on his personal cellular telephone. Three recordings were obtained from the family and examined by a National Transportation Safety Board recorder specialist. The recordings were short, with durations of 11, 21, and 46 seconds respectively.

The first recording began with an inward view showing the individual who was holding the phone and then panned to the rear where the two rear-seat passengers could be seen. The engine sounds indicated that the helicopter was powered on and no abnormal sounds were heard.

The second recording was an outward forward-facing view and captured the helicopter taking off and climbing. The helicopter was adjacent to the left side of a runway. About 10 seconds into the video, the helicopter turned to the left and climbed over trees before flying over a field. No abnormal engine noises were heard.

The third video also captured a predominately outward forward-facing view but panned a few times during the recording. At 2 seconds after the start of the recording, the camera was pointed out of the left side of the helicopter and showed the ground and a parking area with some utility vehicles. At 5 seconds, the camera panned forward and showed the helicopter flying at a low altitude over a tree line. At 15 seconds, the camera panned to the right and captured the instrument panel. The helicopter’s airspeed was 40-45 kts, the altitude read 400 ft, heading was 230°, and the attitude indicator showed a slight left roll. A status bar displayed “GPS” in green, and “MSG” in orange. The annunciator panel was not illuminated with any warnings or cautions. At 22 seconds, the helicopter began a right turn, and the camera captured the turbine power between 97-100% and the rotor rpm between 90-100%. The helicopter’s airspeed was just below 40 kts and the altitude was 400 ft. At 26 seconds, the helicopter continued the right turn. Torque was about 60% and airspeed had slowed to about 35 kts. At 31 seconds, the helicopter had circled the house and began to hover. A left drift occurred as the helicopter yawed to face the backside of the house. At 38 seconds, as the helicopter was behind the house, the torque indicator read about 82% and the airspeed was at 0 kts. At 39 seconds, the torque indicator read about 89% and airspeed read 0 kts. At 46 seconds, the recording ended. At no time during the recoding were any abnormal engine noises heard. The passengers reported that the third video ended seconds before the accident occurred. TESTS AND RESEARCHThe Federal Aviation Administration’s Helicopter Flying Handbook describes Loss of Tail Rotor Effectiveness (LTE) as a condition that occurs “when the flow of air through a tail rotor is altered in some way, either by altering the angle or speed at which the air passes through the rotating blades of the tail rotor system.” This can result in the required thrust from the tail rotor exceeding the thrust available. The Helicopter Flying Handbook further stated regarding LTE:

This alteration of tail rotor thrust can be affected by numerous external factors. The main factors contributing to LTE are:

1. Airflow and downdraft generated by the main rotor blades interfering with the airflow entering the tail rotor assembly.

2. Main blade vortices developed at the main blade tips entering the tail rotor.

3. Turbulence and other natural phenomena affecting the airflow surrounding the tail rotor.

4. A high power setting, hence large main rotor pitch angle, induces considerable main rotor blade downwash and hence more turbulence than when the helicopter is in a low power condition.

5. A slow forward airspeed, typically at speeds where translational lift and translational thrust are in the process of change and airflow around the tail rotor...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22FA086