N8680G

Substantial
Fatal

HARVEY J BROCK TANGO 2S/N: HB101

Accident Details

Date
Saturday, July 30, 2022
NTSB Number
ERA22FA344
Location
Melrose, FL
Event ID
20220730105622
Coordinates
29.749617, -82.026700
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

A loss of control for undetermined reasons.

Aircraft Information

Registration
N8680G
Make
HARVEY J BROCK
Serial Number
HB101
Engine Type
Reciprocating
Year Built
2019
Model / ICAO
TANGO 2ARV1
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GRIDER FIELD SPORT FLIGHT TRAINING INC
Address
405 MELROSE LANDING BLVD
Status
Deregistered
City
HAWTHORNE
State / Zip Code
FL 32640-4422
Country
United States

Analysis

HISTORY OF FLIGHTOn July 30, 2022, about 1005 eastern daylight time, an experimental amateur-built Tango 2 gyroplane, N8680G, was substantially damaged when it was involved in an accident near Melrose, Florida. The flight instructor and pilot under instruction were fatally injured. The gyroplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

On the day of the accident, the flight instructor and pilot under instruction departed Melrose Landing Airport (FD22), Hawthorne, Florida at an unknown time. After the departure from FD22, witnesses observed and heard the gyroplane flying around the local area. One witness captured an image of the gyroplane passing over an auto parts store, and another witness estimated that the gyroplane was operating at an airspeed of 20 to 30 knots, about 1,000 ft above ground level. Just before the accident witnesses also heard additional noises coming from the gyroplane described as banging, whining, and the engine stopping. Some observed debris and objects fall from the sky, with some witnesses describing the loss of propellers, and/or rotor blades. They further described that the gyroplane did not autorotate, but descended rapidly, and was observed to spin, pitch over, tumble, and descend inverted. After impact, smoke and fire was also observed. PERSONNEL INFORMATIONThe flight instructor and pilot under instruction were married to each other. In addition to the gyroplane, they also had an Aeronca 7DC airplane, and a Piper PA-28-160 that they would fly.

Review of pilot logbooks indicated that the pilot under instruction held ratings for airplane single-engine land, and instrument airplane, but did not possess a rating for gyroplanes.

The flight instructor held a flight instructor certificate with a sport rating and endorsements for airplane single-engine land and gyroplane. He had been teaching the pilot under instruction how to fly the gyroplane. At the time of the accident, pilot logbooks indicated that he had given her about 9 hours of instruction in the gyroplane. AIRCRAFT INFORMATIONThe accident aircraft was a gyroplane, which unlike a helicopter did not have a powered rotor. The rotor of the gyroplane would spin in flight due to the air loading on the rotor blades as the gyroplane moved forward. The free spinning rotor of the gyroplane did not require an anti-torque device, such as a tail rotor.

The gyroplane was comprised of an airframe equipped with a 28-ft, two bladed Chenaho rotor, a pre-rotator system, and tricycle type landing gear. It was configured with two seats mounted in a tandem configuration in open cockpits, with an aft-mounted vertical stabilizer and rudder and aft-mounted horizontal stabilizer.

According to Federal Aviation Administration (FAA) and aircraft maintenance records, the gyroplane’s special airworthiness certificate was issued on July 1, 2019. The gyroplane’s most recent condition inspection was completed (about 2 years before the accident) on August 1, 2020. At the time of the accident, the gyroplane and engine had accrued about 77 total hours of operation. AIRPORT INFORMATIONThe accident aircraft was a gyroplane, which unlike a helicopter did not have a powered rotor. The rotor of the gyroplane would spin in flight due to the air loading on the rotor blades as the gyroplane moved forward. The free spinning rotor of the gyroplane did not require an anti-torque device, such as a tail rotor.

The gyroplane was comprised of an airframe equipped with a 28-ft, two bladed Chenaho rotor, a pre-rotator system, and tricycle type landing gear. It was configured with two seats mounted in a tandem configuration in open cockpits, with an aft-mounted vertical stabilizer and rudder and aft-mounted horizontal stabilizer.

According to Federal Aviation Administration (FAA) and aircraft maintenance records, the gyroplane’s special airworthiness certificate was issued on July 1, 2019. The gyroplane’s most recent condition inspection was completed (about 2 years before the accident) on August 1, 2020. At the time of the accident, the gyroplane and engine had accrued about 77 total hours of operation. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed that the gyroplane had impacted a pasture in a nose-low left bank and had come to rest on a magnetic heading of about 243°. Light items such as a seat cushion, flotation cushion, wheel pant, and a stick grip were thrown from the gyroplane during the impact sequence, but there was no wreckage path, and components recovered on scene were within close proximity to the main wreckage.

Examination of the gyroplane revealed that most of the front and rear cockpits were consumed by a postimpact fire. The left main landing gear was embedded in the ground, and the left outboard vertical stabilizer and left horizontal stabilizer were crushed inboard. The center vertical stabilizer and rudder were twisted and wrinkled from the root to the tip, and the right horizontal stabilizer was twisted and wrinkled from the root to the tip.

Flight control continuity was traced from the flight controls in the cockpit through breaks in the flight control system, and to the rudder and rotor head.

Examination of the rotor system revealed that one rotor blade was missing. Further examination revealed that the missing blade had separated about 2 inches outboard of the blade grip and its associated teeter stop (droop stop) was bent in a downward direction. The remaining blade’s droop stop was slightly bent (as compared to the other droop stop), and the blade was bent in two places. It also displayed a black witness mark on the bottom of the blade about 4 ft outboard of the rotor hub (which corresponded to the position of the propeller). The blade also had a blue paint transfer mark on the bottom of the blade about 3 ft inboard of the blade tip (which corresponded to the position of the vertical stabilizer), and areas of damage from the impact sequence along the blade span. The rotor head and hub bar were intact, and the mechanism would rotate and teeter when manipulated by hand.

Examination of the pre-rotator system revealed that it had been damaged during the impact sequence, but continuity was traced from the pre-rotator drive through breaks in the system to the pre-rotator, and it would rotate when turned by hand.

Examination of the three-blade pusher propeller revealed that the propeller hub had remained attached to the propeller speed reduction unit (PSRU). Two of the propeller blades were broken off about 8-inches outboard of the propeller hub. The one remaining blade was intact.

Examination of the PSRU revealed that it still contained oil, and it would rotate by hand. The centrifugal clutch was also intact and did not display any indication of damage.

Examination of the engine revealed that it had remained in its mounts, had received thermal and fire damage, and the drivetrain could not be rotated. The timing chain was intact, and both camshafts were intact and undamaged. All intake and exhaust valves were also intact and no blockages in the exhaust system were discovered.

Oil was present in the engine and oil pump, and the oil pump was functional. The oil filter and internal pleated filter material had been thermally damaged. No metallic debris was found internally. The ignition system and fuel injection system, including the throttle bodies and their associated assemblies, were all fire damaged.

The water pump was intact, but internal examination revealed that the impeller had melted. The radiator was intact and no blockages were discovered.

On August 3, 2022, about 4 days after the accident, the missing rotor blade was discovered in a wooded area about 312 ft east-northeast from the main wreckage.

Materials Laboratory Examination

The separated portion of rotor blade and the rudder push rod were submitted to the National Transportation Safety Board Materials Laboratory for examination.

During the examination, the separated portion of the rotor blade was aligned with its corresponding portion of rotor blade still attached to the rotor head. The alignment followed the curvature of the deformed rotor blade across both sides of the fracture. This alignment exhibited that the rotor blade bent in an upward direction more than 45° before separation.

The fracture surface on the separated portion of the rotor blade exhibited slant fractures consistent with overstress. The upper surface of the rotor blade in proximity to the fracture exhibited ridges consistent with deformation caused by compression. The lower surface of the rotor blade in proximity to the fracture exhibited cracking and stretcher strain marks consistent with deformation caused by tension.

The rudder push-pull rod end exhibited a fracture in the threaded shank right above the nut at the end of the rod. The threaded shank exhibited bending deformation and slant fractures consistent with bending overstress. MEDICAL AND PATHOLOGICAL INFORMATIONFlight Instructor

The Florida 4th District Medical Examiner’s Office performed the flight instructor’s autopsy. According to the flight instructor’s autopsy report, his cause of death was multiple blunt injuries and his manner of death was accident. The extent of injury severely limited structural evaluation of the heart. Moderate aortic atherosclerosis was present and the kidneys exhibited changes that may be seen with chronic high blood pressure. His autopsy did not identify other natural disease.

At the request of the Medical Examiner’s Office, NMS Labs performed toxicological testing of postmortem liver tissue from the flight instructor. NMS labs detected ethanol at 0.27 g/hg in the tested liver tissue.

The FAA Forensic Sciences laboratory also performed toxicological testing of postmortem specimens from the flight instructor. Ethanol was not detected in tested liver or brain tissue specimens. Fentanyl was detected in liver tissue at 0.4 ng/g, in lung tissue at 0.7 ng/g, and in kidney...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA22FA344