N497CA

Substantial
Fatal

CASA C212S/N: 291

Accident Details

Date
Friday, July 29, 2022
NTSB Number
ERA22LA348
Location
Raeford, NC
Event ID
20220801105636
Coordinates
35.030556, -79.236667
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
2

Probable Cause and Findings

The airplane’s encounter with windshear during landing, which resulted in a hard landing and separation of the right main landing gear, and the pilot’s subsequent decision to leave his seat in flight, which resulted in his fall from the airplane.

Aircraft Information

Registration
Make
CASA
Serial Number
291
Engine Type
Turbo-prop
Year Built
1983
Model / ICAO
C212C212
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
28
FAA Model
CN 212-200

Registered Owner (Current)

Name
SPORE LTD LLC
Address
1777 AVIATION WAY
City
COLORADO SPRINGS
State / Zip Code
CO 80916-2707
Country
United States

Analysis

HISTORY OF FLIGHTOn July 29, 2022, about 1404 eastern daylight time, a CASA 212-200 airplane, N497CA, was substantially damaged during a hard landing near Raeford, North Carolina. The pilot-in-command (PIC) was not injured, and the second-in-command (SIC) sustained fatal injuries during the subsequent diversion to Raleigh-Durham International Airport (RDU), Durham, North Carolina. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 skydiving flight.

Federal Aviation Administration (FAA) radar data revealed that the accident flight departed at 1341 and climbed above 13,000 ft mean sea level (msl). According to the PIC, the SIC was flying the airplane and, after unloading the skydivers, he descended to pick up another group of skydivers. The PIC stated that the approach was stabilized until the airplane descended below the tree line and “dropped.” Both pilots called for a go-around maneuver, which the SIC initiated; however, before the SIC could arrest the airplane’s sink rate and initiate a climb, the right main landing gear (RMLG) impacted the runway surface.

The PIC took control of the airplane about 400 ft above ground level and flew a low approach over the runway so that airfield personnel could verify the damage. The personnel subsequently called the PIC to let him know that they recovered the fractured RMLG on the runway. The flight crew contacted air traffic control (ATC) at 1411 and declared an emergency, reported the loss of the right wheel, and requested to divert to RDU. While enroute to RDU, the crew reviewed emergency procedures and planned the landing. During this time, the SIC was primarily responsible for communicating with controllers and reviewing checklist procedures while the PIC flew the airplane. The PIC stated that the SIC was engaged and offered input on runway assignment based on his knowledge of RDU, which the PIC accepted.

Review of ATC information revealed that communications between the SIC and controllers were routine. In his final transmission at 1429, the SIC acknowledged a course heading. The PIC reported that, about this time, which was about 20 minutes into the diversion to RDU, the SIC became visibly upset and repeatedly apologized then said, “I think I am going to be sick.” The PIC described that the SIC opened his side cockpit window, turned his head toward it, and “may have gotten sick.” The PIC took over radio communications, and the SIC lowered the ramp in the back of the airplane, indicating that felt like he was going to be sick and needed air.

The PIC reported that he, “did not find this overly alarming as this (was) a common practice in a hot environment and given our situation.” Subsequently, the PIC stated that the SIC looked at him and stated, “I am sorry,” then disconnected his seat belt, dropped his headset, and ran out the back of the airplane toward the fully open ramp in a headfirst dive. In a radio transmission to ATC about 1 1/2 minutes after the SIC’s radio acknowledgement of the course heading, the PIC notified ATC that the copilot had just “jumped out the back of the plane without a parachute.”

The PIC proceeded on course to RDU, where he performed a low approach and then an

emergency landing. Upon landing, the airplane departed the right side of the runway and

came to rest in the grass. Examination of the accident site by an FAA inspector revealed substantial damage to the RMLG, landing gear fittings, and the airframe structure. PERSONNEL INFORMATIONPilot-in-Command

In an interview with police, the PIC stated he and the SIC met for the first time during this assignment and flew together on the day of the accident as well as the day before. The PIC also served as the Chief Pilot for the operator and had interviewed the SIC when he applied for the pilot position.

Interviews with several company pilots indicated that the PIC was well-liked, knowledgeable, patient, and respected. One company pilot stated that the PIC would never “get into a situation where he corrects an SIC in a manner that makes the situation worse, especially not on an operation.” Another company pilot stated that the PIC was “very approachable. He’s a guy you never want to disappoint. He’s like your dad, and you’d feel bad if you disappointed him. He’s trying to get you to the best and you want to show him your best. He’s not banging on the dash.”

Second-in-Command

The SIC’s family was under the impression that the accident flight was a checkride; however, the operator stated that this was not correct. The SIC’s father stated that his son “could be tough on himself” and that he could see him “being physically sick because of (the loss of the landing gear on the flight with the Chief Pilot).” He also reported that his son had performed a gear-up landing in his previous position as a flight instructor. The operator referenced “internal reports” that indicated that the SIC placed significant professional importance upon a successful flight with the Chief Pilot (the PIC).

Interviews with colleagues and family of the SIC indicated that he was well-liked, happy, smart, and very pleased to be working for the operator. One of the pilots who flew with the SIC stated that:

(The SIC) strove to be near perfect in everything. If we were coming back and we were a few degrees off on the heading, he would chide himself. His approaches were absolutely perfect. I was impressed with his abilities. . . The one thing I noticed is that he wanted to be perfect all the time. He didn’t allow himself any slack.

One time he was so flustered after he dropped the fuel card. He was so upset with himself. “I dropped the card, I can’t believe I dropped the card.” His face was red, and he was sweating. I told him to take 20 minutes to walk to the fuel farm and find it. He RAN to the farm and found it. He was hard on himself, really hard. He knew what the customers needed for a precise product, and he really strove for that and wanted to do a good job. AIRCRAFT INFORMATIONThe CASA C-212 was a turboprop short take-off and landing (STOL) medium-sized cargo plane equipped with two aft doors: the upper cargo door and the ramp door. The cargo door opened upwards and inwards, and the ramp door opened downward and outward. Both were hydraulically-operated from the cockpit via the cargo door handle located directly behind the SIC’s station. Per the Aircraft Flight Manual, the cargo and ramp door are closed for all takeoffs and landings. To allow the skydivers to exit the airplane, the SIC would typically ensure that the ramp surface was level with the cabin floor. In this position, the level cabin floor and ramp surface measured 25 feet, 10 inches from the cockpit bulkhead to end of ramp door. A company pilot stated that, when fully lowered, the downward angle of the ramp door was “very steep” and slippery. The distance from the cockpit bulkhead to where the cabin floor would have dropped off steeply with the ramp fully lowered was about 21.5 feet, about 4 feet closer than the SIC would have been accustomed to seeing the jumpers exit the airplane. A company pilot stated that the SIC had likely never been in the back of the airplane with the ramp lowered. METEOROLOGICAL INFORMATIONThe PIC reported that there was moderate turbulence during the flight. Weather reports along the route of flight to RDU included moderate downdraft convective energy in the area. Additionally, the Severe Weather Gust Potential and Microburst Gust Potential were 50 knots and 57 knots, respectively, along the route of flight. Recorded data downloaded from the flight included vertical load factors supportive of turbulence enroute to RDU. AIRPORT INFORMATIONThe CASA C-212 was a turboprop short take-off and landing (STOL) medium-sized cargo plane equipped with two aft doors: the upper cargo door and the ramp door. The cargo door opened upwards and inwards, and the ramp door opened downward and outward. Both were hydraulically-operated from the cockpit via the cargo door handle located directly behind the SIC’s station. Per the Aircraft Flight Manual, the cargo and ramp door are closed for all takeoffs and landings. To allow the skydivers to exit the airplane, the SIC would typically ensure that the ramp surface was level with the cabin floor. In this position, the level cabin floor and ramp surface measured 25 feet, 10 inches from the cockpit bulkhead to end of ramp door. A company pilot stated that, when fully lowered, the downward angle of the ramp door was “very steep” and slippery. The distance from the cockpit bulkhead to where the cabin floor would have dropped off steeply with the ramp fully lowered was about 21.5 feet, about 4 feet closer than the SIC would have been accustomed to seeing the jumpers exit the airplane. A company pilot stated that the SIC had likely never been in the back of the airplane with the ramp lowered. ADDITIONAL INFORMATIONOn-Board Recorder Information and Ballistics Study

According to ballistic calculations, the SIC left the airplane between 14:31:53 and 14:32:01. A portable wireless receiver on the accident airplane that contained global positioning system (GPS) location data and attitude and heading reference system (AHRS) data was recovered and examined. During the 8-second time frame that the SIC left the airplane, a roll transient and spike in vertical load factor occurred that was an outlier compared to the earlier seven minutes and following three minutes of flight. This event could have been before, during, or after the SIC departed the airplane, and it could not be determined if this roll transient was commanded or a result of external forces on the airplane. MEDICAL AND PATHOLOGICAL INFORMATIONThe North Carolina Office of the Chief Medical Examiner performed the autopsy of the SIC. According to the autopsy report, the cause of death was multiple blunt force injuries, and the manner of death was accident.

Toxicological testing of the SIC’s urine performed by the North Caro...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA22LA348