N22859

Substantial
Fatal

CESSNA 150HS/N: 15068568

Accident Details

Date
Thursday, January 12, 2023
NTSB Number
CEN23FA077
Location
Auburn, NE
Event ID
20230112106566
Coordinates
40.361710, -95.779759
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The flight instructor’s failure to maintain control after a loss of engine power due to carburetor icing while maneuvering for forced landing in dark night visual meteorological conditions.

Aircraft Information

Registration
N22859
Make
CESSNA
Serial Number
15068568
Engine Type
Reciprocating
Model / ICAO
150HC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
FREEMAN JONATHAN T
Address
600 HAZELWOOD DR
Status
Deregistered
City
LINCOLN
State / Zip Code
NE 68510-4324
Country
United States

Analysis

HISTORY OF FLIGHTOn January 11, 2023, about 1924 central standard time, a Cessna 150H, N22859, was substantially damaged when it was involved in an accident near Farington Field Airport (K01), Auburn, Nebraska. The flight instructor and student pilot were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to automatic dependent surveillance-broadcast (ADS-B) information, the airplane departed Lincoln Airport (LNK), Lincoln, Nebraska, about 1845 and climbed to 3,500 ft mean sea level (msl). About 6 miles northwest of K01, the airplane began a descent and the last ADS-B information captured at 19:22:26 showed the airplane about 1.1 miles west of K01 at 105 knots groundspeed and about 1,900 ft msl (see Figure 1).

Figure 1. Airplane’s Flight Track, K01 Airport, and Accident Site

The airplane impacted a field without crops while on a southeasterly heading, about 1.2 miles south of the runway 34 threshold at K01. PERSONNEL INFORMATIONThe flight instructor was issued his initial Federal Aviation Administration (FAA) flight instructor certificate on August 6, 2022, and a flight instructor instrument airplane rating on November 22, 2022. The flight instructor had accumulated about 36 total flight hours at night, and about 12 flight hours instructing students at night. AIRCRAFT INFORMATIONThe cockpit was equipped with flood ‘strip’ lights, which the flight instructor had previously reported could make viewing the in-set instruments in the cockpit more difficult at night (see Figure 2).

Figure 2. Accident Airplane Cockpit Illuminated by Flood Lights METEOROLOGICAL INFORMATIONOn the evening of the accident, United States Naval Observatory data indicated sunset occurred at 1717, the end of civil twilight was at 1747, and moonrise was at 2153 (after the accident). The accident site was surrounded by farm fields with an absence of cultural lighting.

According to the FAA Special Airworthiness Information Bulletin CE-09-35, Carburetor Icing Prevention, the probability of carburetor icing during the weather conditions of the accident was serious at cruise power. AIRPORT INFORMATIONThe cockpit was equipped with flood ‘strip’ lights, which the flight instructor had previously reported could make viewing the in-set instruments in the cockpit more difficult at night (see Figure 2).

Figure 2. Accident Airplane Cockpit Illuminated by Flood Lights WRECKAGE AND IMPACT INFORMATIONThe airplane impacted a field without crops while on a southeasterly heading, about 1.2 miles south of the runway 34 threshold at K01. Ground impressions of the landing gear and crushing of the front fuselage (nose area) were consistent with a near wings level and moderate nose down attitude during impact.

All components of the airplane were observed at the impact site. Flight control continuity was confirmed. The wing flaps and wing flap actuator were both observed in the retracted position. Fuel drained from both wing tanks and the fuel bowl contained no indications of water or sediment.

The propeller spinner was crushed aft, with minimal rotational damage. Both propeller blades were bent aft, with minimal rotational scoring or polishing. The throttle control was observed in a mid-position and was bent, and the mixture control was near the full forward (rich) position. The carburetor heat control was observed in the full forward (off) position.

No evidence of pre-impact mechanical malfunctions were observed during examinations of the engine and airframe that would have precluded normal operation. MEDICAL AND PATHOLOGICAL INFORMATIONAn autopsy was performed on the flight instructor and student pilot by a medical examiner, as directed by the Nemaha County Coroner, Auburn, Nebraska. The cause of death was multiple blunt force injuries.

Toxicology testing of the flight instructor and student pilot performed by the FAA Forensic Sciences Laboratory did not identify any tested-for substances.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN23FA077