N2357

Destroyed
Fatal

HOLLAND TRAVIS E VELOCITYS/N: FGA-001

Accident Details

Date
Saturday, April 15, 2023
NTSB Number
ERA23FA194
Location
Andrews, NC
Event ID
20230415107060
Coordinates
35.183400, -83.880433
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s failure to engage the turbocharger for takeoff and his improper decision to continue the takeoff with partial power, rather than reject the takeoff.

Aircraft Information

Registration
N2357
Make
HOLLAND TRAVIS E
Serial Number
FGA-001
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
VELOCITYBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BENTLEY VELOCITY LLC
Address
1612 N 49TH ST
Status
Deregistered
City
SEATTLE
State / Zip Code
WA 98103-6730
Country
United States

Analysis

HISTORY OF FLIGHTOn April 15, 2023, about 1039 eastern daylight time, an experimental amateur-built Velocity, N2357, was destroyed when it was involved in an accident near Andrews, North Carolina. The commercial pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the current airplane owner, who was the fifth owner, the airplane suffered a landing accident in 2004 and was purchased by a salvage facility. That facility removed the engine and avionics, then sold it to the previous owner, who installed a newly overhauled engine equipped with a turbocharger. The current owner purchased the airplane and installed a new propeller and avionics. At the time of the accident, the engine had about 54 hours of operation since overhaul in 2012. Due to the modifications, a Federal Aviation Administration (FAA) designated airworthiness representative (DAR) inspected the airplane, issued an amended airworthiness certificate with revised operating limitations, and endorsed the airframe logbook on April 1, 2023. The accident flight was the first flight since that endorsement.

The current owner added that he was a private pilot with about 90 hours of flight experience, of which about 10 hours were in the make and model airplane. Since he had little experience, he hired the accident pilot to fly the first flight since the modifications/DAR endorsement. The accident pilot inspected the airplane for about 1.5 hours before the accident takeoff. The owner saw the airplane take off on runway 26, a 5,500-ft-long runway, but subsequently lost sight of it behind buildings.

Witnesses reported that the airplane took off and climbed about 300 ft above ground level while flying a left traffic pattern back to runway 26. Near the crosswind to downwind turn, the engine sounded loud, and the airplane descended into a wooded field and a postcrash fire ensued.

The owner further stated that the engine was equipped with a fixed-pitch cruise propeller. With the turbocharger engaged, the engine would obtain 2,300 rpm; however, with the turbocharger bypassed, the engine would only obtain about 2,050 rpm. A spring switch in the cockpit controlled the turbocharger wastegate, to select whether the turbocharger was engaged or bypassed (or midrange). The owner added that, at 2,050 rpm, the airplane would not be able to fly with one pilot and full fuel, which it had for the accident takeoff.

The owner provided a video that he recorded of a portion of the takeoff. Review of the video revealed that during the takeoff roll the airplane accelerated slower than normal, used more runway than normal, and lifted off the runway in a nose-high attitude. The airplane then descended back to the runway and bounced before lifting off nose-high again toward the end of the runway, where the video ended. PERSONNEL INFORMATIONThe pilot’s logbook was not recovered. On his most recent application for an FAA first class medical certificate, dated February 7, 2018, he reported a total flight experience of 450 hours. WRECKAGE AND IMPACT INFORMATIONThe wreckage came to rest inverted, oriented about a 075° magnetic heading. The left wing was separated and found against a tree inverted at the beginning of the debris path. The main wreckage was at the end of the 50-ft-long debris path and consumed by fire. No cockpit controls or instrumentation was identified.

No seats or restraints were identified. The left aileron and left rudder separated and were recovered near the left wing. The right wing and canard remained with the main wreckage and were consumed by fire. The flight controls consisted of control rods and push-pull tubes. Flight control continuity and trim continuity could not be verified due to fire damage.

The engine came to rest inverted and separated from the airframe. The two-blade propeller remained attached to the hub. One blade appeared undamaged while the other blade exhibited charring and tip separation. The top spark plugs were removed; their electrodes were intact and light gray in color (the Nos. 1 and 3 electrodes were oil soaked).

Borescope examination of the cylinders did not reveal any anomalies. The crankshaft was rotated via an accessory gear drive. Crankshaft, camshaft, and valvetrain continuity were confirmed to the rear accessory section of the engine, and thumb compression was attained on all cylinders. Both magnetos had separated from the engine. One magneto was recovered, and it produced spark at all leads when rotated via electric drill. The other magneto was not located. Due to thermal damage, the fuel system could not be tested. The turbocharger wastegate was found in an open position.

The turbocharger was further examined following wreckage recovery. It exhibited thermal damage, and the turbine would not initially rotate. WD-40 lubricant was applied to the turbine side and compressor side and the unit sat for several minutes. The turbine and its shaft then rotated freely by hand; however, the compressor was melted and did not turn along with the shaft. The compressor side was disassembled for further examination. No scoring was noted on the compressor housing and all compressor wheel blades were intact. The compressor nut was found about two threads loose. The internal housing of the compressor wheel and its corresponding position on the shaft were examined and no rotational scoring was noted. MEDICAL AND PATHOLOGICAL INFORMATIONAn autopsy was performed on the pilot by the North Carolina Office of The Chief Medical Examiner, Raleigh, NC. The cause of death was reported as “multiple blunt force injures.” Toxicological testing was performed on specimens from the pilot by the FAA Office of Forensic Sciences, Oklahoma City, Oklahoma. The results were negative for drugs and alcohol.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23FA194