Accident Details
Probable Cause and Findings
A total loss of power in the right engine due to the right ECU injector wires being severed by the main landing gear actuator piston teeter bar as a result of a lack of clearance and protection of the wiring bundle.
Aircraft Information
Registered Owner (Current)
Analysis
HISTORY OF FLIGHTOn August 01, 2023, at 0930 eastern daylight time, an experimental amateur-built Velocity Twin, N106VT, was substantially damaged when it was involved in an accident near Sandersville, Georgia. The airline transport pilot was seriously injured, and the passenger was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
While returning from airshow in Wisconsin, the pilot stopped at Kaolin Field (OKZ), Sandersville, GA, to have the engines’ valve clearances checked by an authorized repair facility for the engine manufacturer. Upon completion of the valve clearance adjustments and adjustments to the right propeller brush blocks, a ground run was completed, and the engine operated normally. The pilot reported that after completion of all checklists and ground run-ups the takeoff from OKZ was normal. He reported that at 500 ft he initiated his “climb” checklist, during which the right engine “failed hard.” The airplane began to roll to the right and the pilot added left rudder to arrest the roll but was unable; he then added full left aileron, but the airplane continued to roll right. The pilot then performed what he described as a “low yo yo” maneuver and he was able to regain control of the airplane. He reduced throttle on both engines to idle before pitching to maintain 85 kts, which was the simulated single-engine best rate of climb airspeed determined during flight testing. The pilot reported that he was too low to return to the runway and the airplane was not climbing while maintaining 85 knots. After scanning the immediate area, the pilot located a small clearing in a swamp and decided to make a forced landing.
Flight track data recovered from the onboard avionics indicated that the right-engine rpm began to decrease as the airplane reached a GPS altitude of about 600 ft (about 200 ft above ground level). The airplane continued to climb for about 8 seconds, reaching a maximum GPS altitude of about 750 ft. After reaching the maximum altitude the airplane descended for about 7 seconds before leveling around 600 ft GPS altitude for 8 seconds. The airplane then began its final descent until data was lost about 10 seconds later. About 3 seconds after the rpm drop the data showed the airplane begin to bank right about 60° where it remained for about 7 seconds before recovering to near level for about 3 seconds. After leveling, the data shows multiple right banks from between 30° to 60° until the data ends.
The airplane impacted swampy terrain, and the nose of the airplane separated from the impact, resulting in the pilot and passenger being ejected. The airplane was not insured with hull insurance and subsequently was not recovered from the swamp for about one month. Upon examination of the airplane after recovery, it was found that the fuselage, rudder, and both wings were substantially damaged. AIRCRAFT INFORMATIONAccording to Federal Aviation Administration airworthiness records, the airplane was manufactured in 2023 and was built by the pilot. It was powered by 2 ULPower 520T series, 220-horsepower engines equipped with Airmaster AP33 propellers. According to the mechanic who had just completed maintenance on the airplane, it had about 32 hours of total time. He also stated that the pilot came to him in order to have the rest of the initial 15-hour maintenance check completed. The accident flight was the first flight after maintenance.
According to the propeller controller manufacturer, in a scenario where an engine lost combustion, the propeller was windmilling below the set speed, and no change was made to the propeller controller, then the propeller would adjust in the fine direction in an attempt to increase engine speed. AIRPORT INFORMATIONAccording to Federal Aviation Administration airworthiness records, the airplane was manufactured in 2023 and was built by the pilot. It was powered by 2 ULPower 520T series, 220-horsepower engines equipped with Airmaster AP33 propellers. According to the mechanic who had just completed maintenance on the airplane, it had about 32 hours of total time. He also stated that the pilot came to him in order to have the rest of the initial 15-hour maintenance check completed. The accident flight was the first flight after maintenance.
According to the propeller controller manufacturer, in a scenario where an engine lost combustion, the propeller was windmilling below the set speed, and no change was made to the propeller controller, then the propeller would adjust in the fine direction in an attempt to increase engine speed. WRECKAGE AND IMPACT INFORMATIONThe fuselage roof was partially separated from the main fuselage and was cut at the rear attachment to facilitate recovery. The floor was fractured in multiple places. The keel of the fuselage body was fractured just aft of the front seats, forward of the second row of seats. The nose cone was fractured in multiple places. The right canard on the nose was impact-separated, and the left canard was cut to facilitate recovery. The elevators were impact-separated from their respective portions of the canard. The empennage remained attached to the fuselage. The vertical stabilizer remained intact. The rudder was impact-separated from the vertical stabilizer and the rudder control bellcrank was folded forward. The right wing was impact-separated outboard of the engine. The right aileron remained attached to the wing at all attachment points. The left wing was impact-separated outboard of the engine. The left aileron remained attached to the wing at all attachment points. Continuity was confirmed from all flight control surfaces to the flight controls in the cockpit.
The second and third row seating were not occupied during the accident flight and remained attached and in place. The pilot seat was separated from the seat track. The inboard pilot seat track remained attached to the floor at all attachment points; the outboard track remained attached to the floor at the rear attachment point and was separated at the forward attachment point. The four-point pilot seat harness remained attached to the floor at the inboard and rear attachment points; the outboard attachment point was separated. The harness was separated from the pilot’s seat. The front passenger seat’s outboard seat track remained attached to the seat and was separated from the floor. The inboard front passenger seat’s track remained attached to the floor at all attachment points and was separated from the seat. The four-point front passenger seat harness remained attached to the floor at the inboard and rear attachment points; the outboard attachment point was separated. The harness was separated from the front passenger seat.
Both fuel caps remained seated in place. The left-wing fuel tank finger filter remained installed on the stub from the fuselage into the wing fuel tank. Continuity was confirmed from the left and right wing fuel tanks to the header tank installed in the aft fuselage. Both fuel shutoff valves were found in the open position and continuity was established from the header tank through the fuel pumps. The right engine fuel system pre-filters for both the manual and automatic electronic fuel pumps were removed, disassembled, and examined, and exhibited a minor amount of organic debris. The right manual fuel pump was tested by applying power and operated normally. The neutral wire on the right automatic fuel pump was loose in the crimping and was easily pulled free when slightly pulled on. Examination of the disassembled right automatic fuel pump revealed no anomalies. The left-engine automatic and manual fuel pumps were tested by applying power and operated as expected.
The wiring from the engine control unit (ECU) circuit breakers to the aft fuselage were contained inside an undamaged covered channel with multiple other wiring bundles, the main landing gear actuator and teeter bar, and the aileron control tube. The wiring bundles for the right and left ECU were not shielded and were connected with an Adel clamp, along with multiple other wiring bundles, to the inside of the channel. The crimp connection where the wiring loom provided by the engine manufacturer connected to a wiring bundle installed by the pilot/builder, from the left ECU circuit breaker to the left ECU, was found to be loose and the wires were easily pulled out of the crimp connection by hand. One of the left ECU power wires (positive/+ve) was severed in the path of the main landing gear actuator piston; multiple other wires in the left ECU wiring bundle exhibited cuts to the insulation. Both right ECU injector wires (positive/+ve) were severed in the same vicinity as the left ECU wires. Multiple other wires were severed in the same vicinity as those of the right and left ECU wires. The manufacturer reported that with both right ECU injector wires severed, there would be no power to the electronic fuel injectors for the right engine and combustion would stop.
Right Engine
The right-engine crankcase was examined and was intact. Crankshaft continuity was confirmed by rotating the propeller through 720° of rotation. Water and oil were expelled from the engine spark plug holes when the crankshaft was rotated by hand using the propeller. Compression and suction were confirmed on cylinder Nos. 1, 5, and 6 by rotating the propeller. Compression and suction were not observed on cylinder Nos. 2, 3, and 4. The rocker covers were removed from the cylinders and valvetrain continuity was confirmed by rotating the propeller. The Nos. 1, 3, and 6 exhaust valve clearances were not within the range specified by the manufacturer. The Nos. 1, 2, 3, and 4 cylinder heads were removed and the Nos. 2, 3, and 4 exhaust valves were observed to not be seated when compressed air was applied. The turbocharger compressor rotated freely when rotated by hand using a socket wrench. The spark plug wire to ignition coil cap connection...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23LA320