N3HH

Substantial
None

LONG CHARLES JACKSON AVID FLYERS/N: 1066D

Accident Details

Date
Thursday, August 3, 2023
NTSB Number
ERA23LA325
Location
Wetumpka, AL
Event ID
20230804192798
Coordinates
32.543700, -86.211900
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power due to fuel exhaustion because of a leaking fuel drain valve.

Aircraft Information

Registration
Make
LONG CHARLES JACKSON
Serial Number
1066D
Engine Type
Reciprocating
Year Built
1993
Model / ICAO
AVID FLYERBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
AVID FLYER

Registered Owner (Current)

Name
HODGE TYLER A
Address
5141 SABLE CHIME DR
City
WIMAUMA
State / Zip Code
FL 33598-4170
Country
United States

Analysis

On August 3, 2023, at 1326 central daylight time, N3HH, an experimental amateur-built Long Charles Jackson Avid Flyer airplane, sustained substantial damage when it was involved in an accident near Wetumpka, Alabama. The pilot was not injured. The airplane was operated as a 14 Code of Federal Regulations Part 91 personal flight.

The pilot was flying the airplane from Wimauma, Florida, to Wetumpka Airport (08A), Wetumpka, Alabama. The airplane was equipped with a 15-gallon fuel tank located in the wing and the engine consumed about 4.5 gallons of fuel per hour. The pilot said he departed with full fuel and made 4 fuel stops along the route, stopping about every 70-90 minutes. At each stop he filled the fuel tank.

On his third fuel stop, he noted that it took 10 gallons to fill the tank when it should have only taken about 7 gallons. He justified the discrepancy by thinking that he had filled the tanks too quickly on the previous stops, causing the fuel to overflow the cap before it had a chance to settle into the other chambers of the tank.

The pilot then flew to Dawson, Georgia, which was his last fuel stop before landing at 08A. In Dawson, he purchased 6 gallons of fuel. He looked at the airplane’s fuel sight-gauge and it was “full.” Before departure, the pilot took a sample of fuel via the fuel drain valve located under the right wing and it was absent of water. When he took the sample, he observed a few drops of fuel drip from the valve, but no noticeable leaks.

The pilot then departed for 08A. The pilot said that when he was about 6 miles from the airport, about 90 minutes into the flight, the engine began to misfire. The fuel sight tube was completely empty and the clear fuel filter located under the panel was “intermittently gushing fuel.” Seconds later, the engine stopped producing power. The pilot attempted to make a forced landing to a rural gravel road but landed to the right of it and flipped over into a ditch, resulting in substantial damage to the fuselage.

A postaccident examination of the airplane revealed the fuel tank was intact and empty of fuel. No other breaches in the fuel system were observed; however, the fuel drain valve did exhibit blue staining consistent with a leak. Fuel staining was also observed on the right flaperon.

The pilot said that the fuel drain valve had been leaking a few months before the accident. He fixed it by removing the valve and cleaning the O-ring seal, which had a small piece of debris stuck in it from inside the fuel tank. He also flushed the tank with fuel to be sure there was no debris in it. The pilot said that he had not had another problem with the drain valve until the accident flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23LA325