N7748J

Substantial
Minor

PIPER PA-32-260S/N: 32-1152

Accident Details

Date
Monday, December 4, 2023
NTSB Number
ERA24LA054
Location
Millington, TN
Event ID
20231204193467
Coordinates
35.368195, -89.859235
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
1
Total Aboard
2

Probable Cause and Findings

The pilots’ fuel mismanagement during the cross-country flight and incorrect fuel tank selection for the landing approach, which resulted in fuel starvation, a momentary loss of engine power, and collision with terrain short of the runway.

Aircraft Information

Registration
Make
PIPER
Serial Number
32-1152
Engine Type
Reciprocating
Year Built
1969
Model / ICAO
PA-32-260PA32
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
PA-32-260

Registered Owner (Current)

Name
BAS PART SALES LLC
Address
575 ED BEEGLES LN
City
GREELEY
State / Zip Code
CO 80631
Country
United States

Analysis

On December 3, 2023, about 2104 central standard time, a Piper PA-32-260 airplane, N7748J, was substantially damaged when it was involved in an accident near Millington, Tennessee. The private pilot was not injured, and the flight instructor sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the flight instructor, the afternoon and evening involved a roundtrip flight from the airplane’s base airport of Millington/Memphis Airport (NQA), Millington, Tennessee, to Gulf Shores International Airport (JKA), Gulf Shores, Alabama. The private pilot was the pilot flying for both flights, as he was accumulating flight time in his airplane for insurance purposes.

The flight instructor reported that the flight to JKA was uneventful, and they requested that the fixed-base operator ground personnel top off the airplane’s fuel tanks. According to a fuel receipt, 40.3 gallons of fuel were added to the airplane and a top-off was noted.

The flight departed for NQA at 1832 and cruised uneventfully at 4,500 ft mean sea level. While enroute, the pilots switched between the left and right main fuel tanks and did not use the wingtip tanks during cruise. During the approach to land, the before-landing check was completed and the fuel selector was positioned to the left main tank. The instructor recalled that, during the approach, the left and right main inboard tanks indicated a little less than 10 gallons, and the wingtip tanks were indicating full; however, the fuel gauges were “bobbing” throughout the flight.

The flight instructor further reported that, about 500 ft above ground level on final approach to runway 22 with full flaps, the engine suddenly “went quiet” and lost all power. The private pilot continued to fly the airplane, and the flight instructor stated, “best glide” airspeed, which the private pilot continued to maintain. Subsequently, the fuel selector was moved from the left main tank position to the left wingtip tank. Shortly after the fuel tank selector was moved, engine power began increasing; however, nearly simultaneously with this restoration of power, the airplane impacted terrain about 900 ft short of the runway threshold. The private pilot’s statement was consistent with the flight instructor’s description of the loss of engine power and collision with terrain.

According to a Federal Aviation Administration inspector who examined the airplane at the accident site, the fuselage and wings sustained substantial damage. There was no fuel located in either the left main tank or left wingtip tank. About 15 gallons of fuel was drained from the right wingtip tank and about 3 gallons was drained from the right main tank.

Examination of the airplane and engine found no evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation.

The fuel system was evaluated for blockages, with none observed. The left main tank was evaluated for any evidence of leakage, with none observed. The left wingtip tank sustained impact damage and was breached near the leading edge. The right main and wingtip tank were undamaged.

According to the owner’s manual, the airplane was equipped with two inboard main wing fuel tanks that each held 25 gallons, and two outboard wingtip tanks that held 17 gallons of fuel. A fuel selector located on the floor center section of the cockpit enabled a selection of each tank individually, in addition to an OFF position. Fuel was delivered from the tank selected directly to the engine.

The owner’s manual stated that the unusable fuel was about one pint per fuel tank. The owner’s manual further stated with regard to fuel management:

Avoid switching tanks at low altitude since little recovery time is available in event of an error in tank selection. To preclude making a hasty decision, and to provide continuity of flow, the selector should be changed before fuel is exhausted from the tank in use.

The owner’s manual stated that, “The main or tip tank with the highest quantity of fuel should be selected for landing.”

According to the airplane flight manual, one of the placards required to be installed in the airplane stated, “USE MAIN TANKS FIRST.” This placard was present in the accident airplane’s cockpit.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA24LA054