N76TG

Destroyed
None

Glasair Sportsman 2+2S/N: 7278

Accident Details

Date
Thursday, March 14, 2024
NTSB Number
ERA24LA144
Location
Fort Meade, FL
Event ID
20240318193953
Coordinates
27.751523, -81.797227
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot’s inadequate inspection of the airplane following an inflight smoke event, which result in separation of the exhaust pipe and hot exhaust igniting the engine cowling, and a subsequent loss of engine power.

Aircraft Information

Registration
Make
GLASAIR
Serial Number
7278
Engine Type
Reciprocating
Model / ICAO
Sportsman 2+2
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
SPORTSMAN 2+2

Registered Owner (Current)

Name
PAPICH WILLIAM
Address
10192 BOSTON STATE RD
City
BOSTON
State / Zip Code
NY 14025-9749
Country
United States

Analysis

On March 14, 2024, at 1442 eastern daylight time, an experimental, amateur-built Sportsman 2+2, N76TG, was destroyed when it was involved in an accident near Fort Meade, Florida. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

Earlier on the day of the accident, the pilot flew uneventfully from Fly In Ranches Airport (FD25), Vero Beach, Florida to Lakeland Linder International Airport (LAL), Lakeland, Florida. The pilot was later attempting to depart from LAL and described that the outside air temperature was very hot, and that the airplane had idled for longer than he had previously experienced in this time flying it before being cleared to depart. Shortly after takeoff, the pilot smelled a strong “hot” or smoke smell. After conveying his concerns to air traffic control, the pilot returned to the airport and landed. He subsequently taxied, parked the airplane, and shut down the engine. When he opened the engine cowling, he found that a “scat tube” near a header pipe was discolored. He then used a zip tie to secure the tube to an engine mount cross-member, after which he departed on the accident flight, about 1430.

While enroute, about 10 miles away from LAL, smoke entered the cockpit and the engine noise changed. Shortly thereafter, the engine stopped producing power and the pilot performed a forced landing to a field. During the landing, the airplane’s landing gear dug into the ground, and the airplane nosed over coming to rest inverted. The pilot and passenger egressed and the airplane was subsequently consumed by fire.

Postaccident examination of the wreckage by a Federal Aviation Administration inspector revealed that the engine exhaust pipe was missing, and there was evidence of the components in that area having been exposed to extremely high temperatures. Additionally, fire damage was noted on the lower cowling, engine fluid lines, carburetor, and other components beneath the engine. The entire airframe was consumed by fire.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA24LA144