N53EM

Substantial
Minor

BEECH B24RS/N: MC-395

Accident Details

Date
Monday, April 22, 2024
NTSB Number
ERA24LA190
Location
Lumberton Township, NJ
Event ID
20240423194139
Coordinates
39.934278, -74.807222
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot/owner’s failure to ensure adequate maintenance of the airplane, which resulted in a partial loss of engine power during takeoff.

Aircraft Information

Registration
Make
BEECH
Serial Number
MC-395
Engine Type
Reciprocating
Year Built
1976
Model / ICAO
B24RBE24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
B24R

Registered Owner (Current)

Name
CHECKER AIRCRAFT LLC
Address
3511 SILVERSIDE RD STE 105
City
WILMINGTON
State / Zip Code
DE 19810-4902
Country
United States

Analysis

On April 22, 2024, at 1715 eastern daylight time, a Beech B24R, N53EM, sustained substantial damage when it was involved in an accident at the Flying W Airport (N14), Lumberton Township, New Jersey. The pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The pilot/owner said he was taking his airplane get an annual inspection at another airport. He performed a preflight inspection of the airplane, started the engine, and checked the magnetos before departing. Once the airplane became airborne, it did not climb very well and began to settle back towards the ground with the landing gear still extended.

A witness said the airplane’s engine was “sputtering” as it was trying to climb, and sounded like there was a significant drop in rpm. The witness that the airplane subsequently “stalled” and impacted a field off the end of the runway.

A postaccident examination of the airplane revealed that the lower fuselage sustained substantial damage. Examination of the engine revealed low compression on the No. 2 cylinder. The cylinder was examined with a borescope and carbon build-up was noted. The intake valve was not sealing, and the valve seat appeared to be cracked.

A review of the maintenance records revealed the last annual inspection on the engine was completed on May 14, 2014, at a total time of 1,469.2 hours since overhaul. At the time of the accident, the airplane had accrued about 16 hours since the last annual inspection.

Per Federal Aviation Regulation (FAR) 91.409(a), an aircraft must undergo an annual maintenance inspection every 12 calendar months to be legal to operate. 14 CFR Part 43, Appendix D, outlines the scope and detail of items that must be checked during the annual inspection of reciprocating engine aircraft. This regulation is critical for ensuring the airworthiness of aircraft by mandating comprehensive inspections of various systems and components, including the engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA24LA190