N44SN

Substantial
None

BOEING A75N1 (PT17)S/N: 75-2763

Accident Details

Date
Thursday, July 2, 2015
NTSB Number
CEN15LA294
Location
Louisburg, KS
Event ID
20150706X41332
Coordinates
38.562500, -94.625274
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power for reasons that could not be determined during postaccident examinations.

Aircraft Information

Registration
Make
BOEING
Serial Number
75-2763
Engine Type
Reciprocating
Year Built
1941
Model / ICAO
A75N1 (PT17)B752
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
A75N1(PT17)

Registered Owner (Current)

Name
MACARIO MARK A
Address
15612 SE 175TH ST
City
WEIRSDALE
State / Zip Code
FL 32195-3122
Country
United States

Analysis

On July 1, 2015, about 2030 central daylight time, a Boeing A75N1 (PT17) airplane, N44SN, collided with power lines after taking off from Random Ranch Airstrip, Louisburg, Kansas. The pilot, the sole occupant on board, was not injured. The airplane was substantially damaged. The airplane was registered to a private individual in Dakota Dunes, South Dakota, and was being operated by Aircraft Sales, Kansas City, Kansas, under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed. The flight was originating at the time of the accident, and was destined for Miami County Airport (K81) Paola, Kansas.

In a telephone conversation with the National Transportation Safety Board's duty officer, the pilot said the airplane was on consignment by the owner and he had been flying in and out of Random Ranch airstrip, a rural agricultural airstrip, located at 3400 W. 311th Coldwater Rd. He had been demonstrating the airplane to a prospective purchaser. He shut down the engine and he and his passenger disembarked and conversed for a short period of time. The pilot then boarded the airplane, started the engine, and taxied to the south end of the airstrip. He did not perform an engine run-up and did not use carburetor heat, and departed solo to the north. After liftoff and about the midpoint of the 2,000-foot long dry grass runway and at an altitude of 20 to 30 feet above the ground, "it became evident" power was insufficient as the airplane had stopped climbing. He said the engine was turning but it was not producing "as much power." The nose was high and the pilot did not see the approaching power lines. The airplane struck and severed the power lines, nosed down, and impacted a cornfield at the north end of the field.

At the time of the accident, the temperature and dew point recorded at Johnson County Executive Airport (KOJC), Olathe, Kansas, located about 20 miles north of the accident site, were 28 degrees and 24 degrees Celsius (C.), respectively. Plotting these values on the Federal Aviation Administration's (FAA) Special Aviation Information Bulletin (SAIB) CE-09-35 "Carburetor Icing Prevention" chart, the data point lies at the intersection of the blue (icing at glide and cruise power) and green (serious icing at glide power) envelopes. When asked about the possibility of carburetor ice, the pilot said he did not believe it was likely to have been a factor because the hot engine had been shut down for about 30 minutes and it only idled for a couple of minutes before takeoff.

No anomalies were noted during the examination of the airframe and engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN15LA294